QFR No - 8000884335
Defect Details
NC No. | 8000884335 |
NC Date | 26/07/2024 |
NC Submission Date | |
Part No. | F2DZ00912O |
Part Name | FORK BOLT - K8 |
Supplier Name & Code | 101263-SINGLA PRECISION SCREWS |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-OD O/S FITMENT NG |
1. Problem Description
Defect Description | OD O/S |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 11 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@singlaprecision.com |
Plant Head/CEO Email ID | quality@singlaprecision.com |
MD Email ID | aditya@singlaprecision.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
540
|
0
|
0
|
2000
|
2000
|
4540
|
Check Qty |
540
|
0
|
0
|
2000
|
2000
|
4540
|
NG Qty |
11
|
0
|
0
|
0
|
0
|
11
|
Scrap | 11 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
We Checked 100% material lying at Various stage |
3. Process Flow
Process Flow Description |
---|
Raw material +Part off +Drilling +Punching +Drilling +Tapping +CNC Machine +Rolling +Re-Tapping +Finish +Final Inspection +Packing |
4. Process Details
Process / Operation | Punching |
Outsource | Yes |
Machine / Cell | Punching |
Machine / Cell No. | 01 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Material to Swell in Punching Process | Validation And Found NG | X |
Material | RM GRADE AND SIZE NOT OK | VALIDATION ANF FOUND OK | O |
Man | UNAWARENESS OF OPERATOR | VALIDATION AND FOUND OPERATOR SKILL LEVEL LOW | X |
Tool | Punching tool wear out | Validation and Found OK | O |
Method | Forging Part checking gauge not effective | Validation And Found NG | X |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | sampling |
7. Root Cause Analysis (Occurance)
Why 1 | NOT AS PER SPECIFICATION-OD |
Why 2 | Material to swell in Punching process |
Why 3 | After Punching Process not CLG Process Add |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | CLG operation not add after Punching process |
Root Cause Analysis (Outflow)
Why 1 | NOT AS PER SPECIFICATION-OD |
Why 2 | Inspection Plan was not Effective |
Why 3 | final inspection standard checking Frequency change 100% Gauge implements |
Why 4 | As per sampling Plan part checking in final inspection |
Why 5 | Ng part skipped from inspection and machine |
Root Cause (Outflow) | final inspection standard checking Frequency change 100% Gauge implements |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | final inspection standard checking Frequency change 100% Gauge implements | Mr Ganesh Maurya | 31/07/2024 | 01/08/2024 | Completed |
Occurance | CLG operation not add after Punching process | Mr Ganesh Maurya | 31/07/2024 | 01/08/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | final inspection standard checking Frequency change OD -100% Gauge implements |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 |
10. Evidance of Countermeasure
Occurance (Before) |
CLG operation not add after Punching process 975_Occurance_Before.jpeg |
Occurance (After) |
CLG operation add after Punching process 975_Occurance_After.jpeg |
Outflow (Before) |
Final Inspection standards as per sampling plan 975_Outflow_Before.jpeg |
Outflow (After) |
Final Inspection standards 100% OD Dia checked 975_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | clg machine -01 |
12. Document Review
Documents | Drawing |
Specify Other Document | PFMEA ,Final insp St |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | 5. Problem Analysis - Need all 4M 7. Root Cause Analysis (Occurance & Outflow) - Not clear |