QFR No - 8000884338
Defect Details
NC No. 8000884338
NC Date 26/07/2024
NC Submission Date
Part No. 520HL00202
Part Name OIL LOCK COLLAR
Supplier Name & Code 100176-GKN SINTER METALS PRIVATE LIMI
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-CRACK
 
1. Problem Description
Defect Description Crack
Detection Stage Inprocess
Problem Severity Safety
NG Quantity 1
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID Rajendra.Sethiya@gknpm.com
Plant Head/CEO Email ID Pratik.Dharangaonkar@gknpm.com
MD Email ID Rajesh.Mirani@gknpm.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
7642
8000
0
0
0
15642
Check Qty
7642
8000
0
0
0
15642
NG Qty
1
0
0
0
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
Quality Alert raised at In process area. Awareness training given to all concerned stakeholders . All stock is under hold for verification
 
3. Process Flow
Process Flow Description
Mixing-Forming-Sintering-steam treatment -PDI to Post FG
 
4. Process Details
Process / Operation Forming
Outsource No
Machine / Cell Small Segemnt
Machine / Cell No. Plant 1
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManNew OpeartorOperator Skill Matrix verifiedO
MethodPart fallen on Rotary table due to conveyor height MismatchPast History of Concerned batch verified observed Excess gap creating Impact on ODX
MaterialWrong MixMTRO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Sampling Inspection
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size 5
7. Root Cause Analysis (Occurance)
Why 1 Crack Generated on OD During forming process
Why 2 Impact Generated on Part OD on Rotary table during TRansferring From conveyor
Why 3 Excess gap between rotary table & conveyor chute End
Why 4 No checkpoint to verify gap
Why 5
Root Cause (Occurance) Excess gap between Rotary table & Conveyor chute end resulted into excess impact on Part OD
 
Root Cause Analysis (Outflow)
Why 1 Crack parts outflown to ETL
Why 2 Crack parts not detected during Inspection
Why 3 Inspection frequency not adequate
Why 4 Inspection done on sampling basis
Why 5
Root Cause (Outflow) Inspection done on sampling basis
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceGlide path provided between Rotary table & Conveyor Clearence to avoid impactRohan G30/07/202430/07/2024Completed
OutflowInspection Frequency revised from 5 Parts/4 hour to 5 Parts/ 1hourRohan G30/07/202430/07/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Inspection Frequency revised from 5 Parts/8 hour to 5 parts/ 1 hour
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 10 Nos
10. Evidance of Countermeasure
Occurance (Before) Excess gap on Rotary table
978_Occurance_Before.pptx
Occurance (After) Gap eliminated to avoid stuck up issue
978_Occurance_After.pptx
Outflow (Before) Before Inspection frequency 5 Parts/8 hour
978_Outflow_Before.pdf
Outflow (After) After Inspection Frequency 5 Parts/ 1 Hour
978_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents ControlPlan, PFMEA
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 50
Reason for submission OK