QFR No - 8000884570
Defect Details
NC No. | 8000884570 |
NC Date | 29/07/2024 |
NC Submission Date | |
Part No. | 080FA04433 |
Part Name | FORK PIPE MACHINED - CT100 |
Supplier Name & Code | 101223-SANGKAJ BRIGHT WIRES PRIVATE L |
ETL Plant | 1146-ETL Suspension Narasapura |
Defect Details | DRILL OUT-DOUBLE DRILL |
1. Problem Description
Defect Description | CT 100 FROK PIPE DOUBLE DRILL ISSUE |
Detection Stage | Inprocess |
Problem Severity | Function |
NG Quantity | 1 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | mayursurse11@gmail.com |
Plant Head/CEO Email ID | steel@sangkaj.com |
MD Email ID | anirudh.2007@hotmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1000
|
0
|
0
|
2000
|
0
|
3000
|
Check Qty |
999
|
0
|
0
|
2000
|
0
|
2999
|
NG Qty |
1
|
0
|
0
|
0
|
0
|
1
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% Segregation at ETL End |
3. Process Flow
Process Flow Description |
---|
Recipe Raw material + Incoming RM inspection + CNC1ST Turning + CNC 2nd Turning + Drilling + Air Cleaning + Final Inspection + PDI + Dispatch |
4. Process Details
Process / Operation | Drilling |
Outsource | No |
Machine / Cell | Drill cell |
Machine / Cell No. | Drill mc no 1 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Fixture loose condition found | not ok found | O |
Man | Lack of operator awareness | traing not doen | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 nos |
7. Root Cause Analysis (Occurance)
Why 1 | DRILL OUT-DOUBLE DRILL |
Why 2 | At the time of drill all material ok |
Why 3 | but 1 part drill fixture loose condition |
Why 4 | Fixture loss condition |
Why 5 | |
Root Cause (Occurance) | Fixture loss condition |
Root Cause Analysis (Outflow)
Why 1 | DRILL OUT-DOUBLE DRILL |
Why 2 | Inspection as a sampling basis |
Why 3 | Inspection Done On Sampling Basis. (5 Nos / Lot) |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Inspection Done On Sampling Basis. (5 Nos / Lot) |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Fixture loss condition found due to Hourly check to fixture tight | Mr Pratap | 04/08/2024 | 05/08/2024 | Completed |
Occurance | At the time NG Produce operator kept red bin,training to operator | Mr Mayur | 04/08/2024 | 05/08/2024 | Completed |
Outflow | Check point added final inspection* aware to operator | Mr Mayur | 03/08/2024 | 05/08/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | No change |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 nos |
10. Evidance of Countermeasure
Occurance (Before) |
Weekly PM NOT DONE JULY MONTH 993_Occurance_Before.png |
Occurance (After) |
PM DONE STILL DATE 993_Occurance_After.jpg |
Outflow (Before) |
Training not done 993_Outflow_Before.png |
Outflow (After) |
Training done opearator & inspector 993_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All model |
12. Document Review
Documents | PMCheckSheet, WISOP |
Specify Other Document | no |
13. Effectiveness Of Action
Reviewed Quantity | 5000 |
Reason for submission | Reviewed next two lots found ok |