QFR No - 8000884570
Defect Details
NC No. 8000884570
NC Date 29/07/2024
NC Submission Date
Part No. 080FA04433
Part Name FORK PIPE MACHINED - CT100
Supplier Name & Code 101223-SANGKAJ BRIGHT WIRES PRIVATE L
ETL Plant 1146-ETL Suspension Narasapura
Defect Details DRILL OUT-DOUBLE DRILL
 
1. Problem Description
Defect Description CT 100 FROK PIPE DOUBLE DRILL ISSUE
Detection Stage Inprocess
Problem Severity Function
NG Quantity 1
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID mayursurse11@gmail.com
Plant Head/CEO Email ID steel@sangkaj.com
MD Email ID anirudh.2007@hotmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
0
0
2000
0
3000
Check Qty
999
0
0
2000
0
2999
NG Qty
1
0
0
0
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
100% Segregation at ETL End
 
3. Process Flow
Process Flow Description
Recipe Raw material + Incoming RM inspection + CNC1ST Turning + CNC 2nd Turning + Drilling + Air Cleaning + Final Inspection + PDI + Dispatch
 
4. Process Details
Process / Operation Drilling
Outsource No
Machine / Cell Drill cell
Machine / Cell No. Drill mc no 1
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManFixture loose condition foundnot ok foundO
ManLack of operator awarenesstraing not doenO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5 nos
7. Root Cause Analysis (Occurance)
Why 1 DRILL OUT-DOUBLE DRILL
Why 2 At the time of drill all material ok
Why 3 but 1 part drill fixture loose condition
Why 4 Fixture loss condition
Why 5
Root Cause (Occurance) Fixture loss condition
 
Root Cause Analysis (Outflow)
Why 1 DRILL OUT-DOUBLE DRILL
Why 2 Inspection as a sampling basis
Why 3 Inspection Done On Sampling Basis. (5 Nos / Lot)
Why 4
Why 5
Root Cause (Outflow) Inspection Done On Sampling Basis. (5 Nos / Lot)
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceFixture loss condition found due to Hourly check to fixture tightMr Pratap04/08/202405/08/2024Completed
OccuranceAt the time NG Produce operator kept red bin,training to operatorMr Mayur04/08/202405/08/2024Completed
OutflowCheck point added final inspection* aware to operatorMr Mayur03/08/202405/08/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details No change
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5 nos
10. Evidance of Countermeasure
Occurance (Before) Weekly PM NOT DONE JULY MONTH
993_Occurance_Before.png
Occurance (After) PM DONE STILL DATE
993_Occurance_After.jpg
Outflow (Before) Training not done
993_Outflow_Before.png
Outflow (After) Training done opearator & inspector
993_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All model
 
12. Document Review
Documents PMCheckSheet, WISOP
Specify Other Document no
 
13. Effectiveness Of Action
Reviewed Quantity 5000
Reason for submission Reviewed next two lots found ok