QFR No - 8000884574
Defect Details
NC No. | 8000884574 |
NC Date | 29/07/2024 |
NC Submission Date | |
Part No. | F2FA19033M |
Part Name | K0PG FORK PIPE MACHINED |
Supplier Name & Code | 101223-SANGKAJ BRIGHT WIRES PRIVATE L |
ETL Plant | 1146-ETL Suspension Narasapura |
Defect Details | LENGTH UNDERSIZE-HEIGHT LESS |
1. Problem Description
Defect Description | K0PG FORK PIPE TOTAL LENGTH LESS ISSUE |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 1 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | mayursurse11@gmail.com |
Plant Head/CEO Email ID | steel@sangkaj.com |
MD Email ID | anirudh.2007@hotmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
2000
|
0
|
0
|
1000
|
0
|
3000
|
Check Qty |
1999
|
0
|
0
|
1000
|
0
|
2999
|
NG Qty |
1
|
0
|
0
|
0
|
0
|
1
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% Inspection ETL & WIP STOCK |
3. Process Flow
Process Flow Description |
---|
Recipe Raw material + Incoming RM inspection + CNC1ST Turning + CNC 2nd Turning + Drilling + Air Cleaning + Final Inspection + PDI + Dispatch |
4. Process Details
Process / Operation | CNC 2ND SIDE |
Outsource | No |
Machine / Cell | CNC CELL |
Machine / Cell No. | 4 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Clamping not proper rest | Clamping rest Judgement error | O |
6. Inspection Method Analysis (Current)
Inspection Method | Sp. Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 5nos |
7. Root Cause Analysis (Occurance)
Why 1 | Total Height undersize |
Why 2 | Not proper part rest on stopper |
Why 3 | At inside of collet stuck loose burr |
Why 4 | No arrangement to clean stopper & collet |
Why 5 | |
Root Cause (Occurance) | No arrangement to clean stopper & collet |
Root Cause Analysis (Outflow)
Why 1 | Total Height undersize |
Why 2 | Rejected material mix-up with ok material |
Why 3 | Rejection bin provided but not daily rejection rework clear |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Rejection bin provided but not daily rejection rework clear |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | No arrangement to clean stopper & collet | Mayur | 02/08/2024 | 04/08/2024 | Completed |
Outflow | Rejection bin provided but not daily rejection rework clear | Supervisor | 04/08/2024 | 03/08/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | no change |
Inspection Method | Sp. Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 5nos |
10. Evidance of Countermeasure
Occurance (Before) |
Air not available at CNC stage 992_Occurance_Before.jpg |
Occurance (After) |
Air available at CNC stage to clean collet loose burr 992_Occurance_After.jpg |
Outflow (Before) |
Opl not displayed 992_Outflow_Before.png |
Outflow (After) |
OPL DISPLAYED 992_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | ALL MODEL |
12. Document Review
Documents | WISOP |
Specify Other Document | OPL DISPLAYED |
13. Effectiveness Of Action
Reviewed Quantity | 1000 |
Reason for submission | verified next lots found ok no issue |