QFR No - 8000884574
Defect Details
NC No. 8000884574
NC Date 29/07/2024
NC Submission Date
Part No. F2FA19033M
Part Name K0PG FORK PIPE MACHINED
Supplier Name & Code 101223-SANGKAJ BRIGHT WIRES PRIVATE L
ETL Plant 1146-ETL Suspension Narasapura
Defect Details LENGTH UNDERSIZE-HEIGHT LESS
 
1. Problem Description
Defect Description K0PG FORK PIPE TOTAL LENGTH LESS ISSUE
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 1
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID mayursurse11@gmail.com
Plant Head/CEO Email ID steel@sangkaj.com
MD Email ID anirudh.2007@hotmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2000
0
0
1000
0
3000
Check Qty
1999
0
0
1000
0
2999
NG Qty
1
0
0
0
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
100% Inspection ETL & WIP STOCK
 
3. Process Flow
Process Flow Description
Recipe Raw material + Incoming RM inspection + CNC1ST Turning + CNC 2nd Turning + Drilling + Air Cleaning + Final Inspection + PDI + Dispatch
 
4. Process Details
Process / Operation CNC 2ND SIDE
Outsource No
Machine / Cell CNC CELL
Machine / Cell No. 4
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManClamping not proper restClamping rest Judgement errorO
 
6. Inspection Method Analysis (Current)
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 5nos
7. Root Cause Analysis (Occurance)
Why 1 Total Height undersize
Why 2 Not proper part rest on stopper
Why 3 At inside of collet stuck loose burr
Why 4 No arrangement to clean stopper & collet
Why 5
Root Cause (Occurance) No arrangement to clean stopper & collet
 
Root Cause Analysis (Outflow)
Why 1 Total Height undersize
Why 2 Rejected material mix-up with ok material
Why 3 Rejection bin provided but not daily rejection rework clear
Why 4
Why 5
Root Cause (Outflow) Rejection bin provided but not daily rejection rework clear
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceNo arrangement to clean stopper & colletMayur02/08/202404/08/2024Completed
OutflowRejection bin provided but not daily rejection rework clearSupervisor04/08/202403/08/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details no change
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 5nos
10. Evidance of Countermeasure
Occurance (Before) Air not available at CNC stage
992_Occurance_Before.jpg
Occurance (After) Air available at CNC stage to clean collet loose burr
992_Occurance_After.jpg
Outflow (Before) Opl not displayed
992_Outflow_Before.png
Outflow (After) OPL DISPLAYED
992_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant ALL MODEL
 
12. Document Review
Documents WISOP
Specify Other Document OPL DISPLAYED
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission verified next lots found ok no issue