QFR No - 8000884592
Defect Details
NC No. 8000884592
NC Date 30/07/2024
NC Submission Date
Part No. 550DZ05202
Part Name FORK BOLT :PRFH-006
Supplier Name & Code 100106-SHARP ENGINEERS.
ETL Plant 1146-ETL Suspension Narasapura
Defect Details THREADING NOT OK-MINOR DIA GO NOT ANSWERING
 
1. Problem Description
Defect Description FORK BOLT M10 THREAD MINOR DIA PLUG GAUGE GO NOT ANSWERING
Detection Stage Receipt
Problem Severity Safety
NG Quantity 139
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@apw3.co.in
Plant Head/CEO Email ID kurund.ma@sharp-engineers.com
MD Email ID urkhandelwal@sharp-engineers.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
3000
0
0
2500
3500
9000
Check Qty
3000
0
0
2500
3500
9000
NG Qty
139
0
0
5
3
147
 
Scrap 147
Rework 0
Under Deviation 0
Containment Action
Segregation done immediately for all suspected material of pipeline.
 
3. Process Flow
Process Flow Description
RM incoming-Parting and drilling-Tipm grinding-CNC 1st-Pre thread drilling and tapping-OD grinding - thread rolling-Tapping -Plating-final inspection-Pre dispatch inspection-packing and forwarding
 
4. Process Details
Process / Operation Tapping
Outsource No
Machine / Cell Tapping
Machine / Cell No. Tapping
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManNew operatorExperienced operator is workingO
ManUnskilled operatorOperator available as per skill matrix.O
MethodWrong settingSetting done okO
ToolWrong toolTool found okO
MachineProcess parameter changefound as per specificationO
MethodChecking MethodVerified and found okO
MachinePlating thicknessfound plating thickness oversizeX
MaterialMaterial grade changefound as per specificationO
MaterialMaterial hardnessas per specification foundO
ToolWear outfound okO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5
7. Root Cause Analysis (Occurance)
Why 1 M10 THREAD MINOR DIA PLUG GAUGE GO NOT ANSWERING
Why 2 Minor Dia Undersize
Why 3 Undersize by 20micron
Why 4 Found Excess of plating
Why 5 Barrel time increased due to manual dependency
Root Cause (Occurance) Barrel time increased due to manual dependency
 
Root Cause Analysis (Outflow)
Why 1 M10 THREAD MINOR DIA PLUG GAUGE GO NOT ANSWERING
Why 2 Skip from inspection
Why 3 Inspection frequency is less
Why 4 Inspection frequency is 10 nos per lot
Why 5
Root Cause (Outflow) Inspection frequency is 10 nos per lot
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceStarted production on Auto line to avoid Excess of plating due to timingMr. Pradeep Bhagwat14/08/202414/08/2024Completed
OutflowInspection frequency was increased to 20 nos per lot, also started 100% of inspection before dispatchedMr. Omkar Bhange14/08/202414/08/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Inspection frequency was increased to 20 nos per lot,
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Barrel time increased due to manual dependency
989_Occurance_Before.jpeg
Occurance (After) Started production on Auto line
989_Occurance_After.jpeg
Outflow (Before) Inspection frequency is 10 nos per lot and sampling inspection.
989_Outflow_Before.jpg
Outflow (After) Inspection frequency is 20 nos per lot also started 100% gauge inspection before dispatch.
989_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 5000
Reason for submission reviewed next 2 lots found ok