QFR No - 8000884592
Defect Details
NC No. | 8000884592 |
NC Date | 30/07/2024 |
NC Submission Date | |
Part No. | 550DZ05202 |
Part Name | FORK BOLT :PRFH-006 |
Supplier Name & Code | 100106-SHARP ENGINEERS. |
ETL Plant | 1146-ETL Suspension Narasapura |
Defect Details | THREADING NOT OK-MINOR DIA GO NOT ANSWERING |
1. Problem Description
Defect Description | FORK BOLT M10 THREAD MINOR DIA PLUG GAUGE GO NOT ANSWERING |
Detection Stage | Receipt |
Problem Severity | Safety |
NG Quantity | 139 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@apw3.co.in |
Plant Head/CEO Email ID | kurund.ma@sharp-engineers.com |
MD Email ID | urkhandelwal@sharp-engineers.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
3000
|
0
|
0
|
2500
|
3500
|
9000
|
Check Qty |
3000
|
0
|
0
|
2500
|
3500
|
9000
|
NG Qty |
139
|
0
|
0
|
5
|
3
|
147
|
Scrap | 147 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Segregation done immediately for all suspected material of pipeline. |
3. Process Flow
Process Flow Description |
---|
RM incoming-Parting and drilling-Tipm grinding-CNC 1st-Pre thread drilling and tapping-OD grinding - thread rolling-Tapping -Plating-final inspection-Pre dispatch inspection-packing and forwarding |
4. Process Details
Process / Operation | Tapping |
Outsource | No |
Machine / Cell | Tapping |
Machine / Cell No. | Tapping |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | New operator | Experienced operator is working | O |
Man | Unskilled operator | Operator available as per skill matrix. | O |
Method | Wrong setting | Setting done ok | O |
Tool | Wrong tool | Tool found ok | O |
Machine | Process parameter change | found as per specification | O |
Method | Checking Method | Verified and found ok | O |
Machine | Plating thickness | found plating thickness oversize | X |
Material | Material grade change | found as per specification | O |
Material | Material hardness | as per specification found | O |
Tool | Wear out | found ok | O |
6. Inspection Method Analysis (Current)
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 |
7. Root Cause Analysis (Occurance)
Why 1 | M10 THREAD MINOR DIA PLUG GAUGE GO NOT ANSWERING |
Why 2 | Minor Dia Undersize |
Why 3 | Undersize by 20micron |
Why 4 | Found Excess of plating |
Why 5 | Barrel time increased due to manual dependency |
Root Cause (Occurance) | Barrel time increased due to manual dependency |
Root Cause Analysis (Outflow)
Why 1 | M10 THREAD MINOR DIA PLUG GAUGE GO NOT ANSWERING |
Why 2 | Skip from inspection |
Why 3 | Inspection frequency is less |
Why 4 | Inspection frequency is 10 nos per lot |
Why 5 | |
Root Cause (Outflow) | Inspection frequency is 10 nos per lot |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Started production on Auto line to avoid Excess of plating due to timing | Mr. Pradeep Bhagwat | 14/08/2024 | 14/08/2024 | Completed |
Outflow | Inspection frequency was increased to 20 nos per lot, also started 100% of inspection before dispatched | Mr. Omkar Bhange | 14/08/2024 | 14/08/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Inspection frequency was increased to 20 nos per lot, |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Barrel time increased due to manual dependency 989_Occurance_Before.jpeg |
Occurance (After) |
Started production on Auto line 989_Occurance_After.jpeg |
Outflow (Before) |
Inspection frequency is 10 nos per lot and sampling inspection. 989_Outflow_Before.jpg |
Outflow (After) |
Inspection frequency is 20 nos per lot also started 100% gauge inspection before dispatch. 989_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NA |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP |
Specify Other Document | NA |
13. Effectiveness Of Action
Reviewed Quantity | 5000 |
Reason for submission | reviewed next 2 lots found ok |