QFR No - 8000884639
Defect Details
NC No. | 8000884639 |
NC Date | 30/07/2024 |
NC Submission Date | |
Part No. | S1AB00612B |
Part Name | ADJUSTER PLATED |
Supplier Name & Code | 100782-NICE STEEL INDUSTRIES |
ETL Plant | 1146-ETL Suspension Narasapura |
Defect Details | WELDING NOT OK-IMPROPER WELDING |
1. Problem Description
Defect Description | Adjuster improper welding defects issue |
Detection Stage | Receipt |
Problem Severity | Safety |
NG Quantity | 1386 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo | nukwu5cfxpybz1b4adopzotb.jpg |
Supplier Communication Details
Quality Head Email ID | ppc.nice@batragroup.biz |
Plant Head/CEO Email ID | ho.nice@batragroup.biz |
MD Email ID | hitesh@batragroup.biz |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1000
|
0
|
0
|
2000
|
1000
|
4000
|
Check Qty |
1000
|
0
|
0
|
2000
|
1000
|
4000
|
NG Qty |
10
|
0
|
0
|
50
|
10
|
70
|
Scrap | 0 |
Rework | 70 |
Under Deviation | 0 |
Containment Action |
---|
1- Stock checked at Nice end . 2- Training provided to inspection team about visual defects 3- Quality gate implemented to control the out flow of parts. 4-One point lesson displayed at quality table . |
3. Process Flow
Process Flow Description |
---|
10 RECEIVING INSPECTION 20 STORAGE 30 BLANKING 40 1st BENDING ( `U` BENDING) 50 FINAL BENDING ( ROUNDING ) 60 MIG WELDING 70 FLAIRING 1st 80 FLAIRING 2nd 90 ID SIZING 100 SIDE GRINDING & BUFFING 110 REROUNDING 120 BROACHING 130 HEAD GRINDING 140 OUTSIDE MOVEMENT FOR PLATING 150 STORAGE & RQC INSP. OF PLATED MATERIAL 160 FINAL INSPECTION 170 PACKING & DISPATCH |
4. Process Details
Process / Operation | WELDING |
Outsource | No |
Machine / Cell | MIG WELDING |
Machine / Cell No. | 10,11 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | UNSKILLED MANPOWER WAS DEPUTED AT WELDING | SKILLED MANPOWER WAS AVAILABLE AND SKILL MATRIX VERIFIED | O |
Material | WRONG MATERIAL USED | MTC VERIFIED | O |
Machine | HIGHER/LOWER CAPACITY MACHINE USED | MACHINED VERIFIED AND FOUND OK | O |
Tool | Gap of Joint is over size | Gap not maintained during rounding | X |
Method | PROCESS PARAMETER CHANGED | CHECKED AND FOUND OK | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | BY DVC |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | VISUAL |
7. Root Cause Analysis (Occurance)
Why 1 | Part crack at one side from gap due to One side welding was not proper in part gap |
Why 2 | One side welding was over fill and other side was uneven welding |
Why 3 | Gap of Joint is over size |
Why 4 | Gap not maintained during rounding |
Why 5 | Error in Rounding operation |
Root Cause (Occurance) | 1-Gap of Joint is over size 2-Error in Rounding operation |
Root Cause Analysis (Outflow)
Why 1 | Defective part passed at customer end |
Why 2 | Defective part not detected by inspector |
Why 3 | Inspector was not followed the WI |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Defective part not detected by inspector |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | 200% inspection started | Nice Steel Ind. | 31/07/2024 | 01/08/2024 | Completed |
Occurance | Die design changed and now Gap to be provided in tapper in die | Nice Steel | 01/08/2024 | 01/08/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 200% visual inspection started |
Inspection Method | Other |
Other Inspection Method | 200% |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 200% |
10. Evidance of Countermeasure
Occurance (Before) |
Tool design 980_Occurance_Before.png |
Occurance (After) |
Tool design 980_Occurance_After.png |
Outflow (Before) |
NO DOCUMENT 980_Outflow_Before.png |
Outflow (After) |
OPL 980_Outflow_After.png |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NOT APPLICABLE |
12. Document Review
Documents | WISOP |
Specify Other Document | OPL |
13. Effectiveness Of Action
Reviewed Quantity | 1000 |
Reason for submission | still we are receiving the welding issues |