QFR No - 8000884639
Defect Details
NC No. 8000884639
NC Date 30/07/2024
NC Submission Date
Part No. S1AB00612B
Part Name ADJUSTER PLATED
Supplier Name & Code 100782-NICE STEEL INDUSTRIES
ETL Plant 1146-ETL Suspension Narasapura
Defect Details WELDING NOT OK-IMPROPER WELDING
 
1. Problem Description
Defect Description Adjuster improper welding defects issue
Detection Stage Receipt
Problem Severity Safety
NG Quantity 1386
Is Defect Repeatative? Yes
Defect Sketch / Photo nukwu5cfxpybz1b4adopzotb.jpg
Supplier Communication Details
Quality Head Email ID ppc.nice@batragroup.biz
Plant Head/CEO Email ID ho.nice@batragroup.biz
MD Email ID hitesh@batragroup.biz
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
0
0
2000
1000
4000
Check Qty
1000
0
0
2000
1000
4000
NG Qty
10
0
0
50
10
70
 
Scrap 0
Rework 70
Under Deviation 0
Containment Action
1- Stock checked at Nice end . 2- Training provided to inspection team about visual defects 3- Quality gate implemented to control the out flow of parts. 4-One point lesson displayed at quality table .
 
3. Process Flow
Process Flow Description
10 RECEIVING INSPECTION 20 STORAGE 30 BLANKING 40 1st BENDING ( `U` BENDING) 50 FINAL BENDING ( ROUNDING ) 60 MIG WELDING 70 FLAIRING 1st 80 FLAIRING 2nd 90 ID SIZING 100 SIDE GRINDING & BUFFING 110 REROUNDING 120 BROACHING 130 HEAD GRINDING 140 OUTSIDE MOVEMENT FOR PLATING 150 STORAGE & RQC INSP. OF PLATED MATERIAL 160 FINAL INSPECTION 170 PACKING & DISPATCH
 
4. Process Details
Process / Operation WELDING
Outsource No
Machine / Cell MIG WELDING
Machine / Cell No. 10,11
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManUNSKILLED MANPOWER WAS DEPUTED AT WELDINGSKILLED MANPOWER WAS AVAILABLE AND SKILL MATRIX VERIFIEDO
MaterialWRONG MATERIAL USEDMTC VERIFIEDO
MachineHIGHER/LOWER CAPACITY MACHINE USEDMACHINED VERIFIED AND FOUND OKO
ToolGap of Joint is over sizeGap not maintained during roundingX
MethodPROCESS PARAMETER CHANGEDCHECKED AND FOUND OKO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method BY DVC
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size VISUAL
7. Root Cause Analysis (Occurance)
Why 1 Part crack at one side from gap due to One side welding was not proper in part gap
Why 2 One side welding was over fill and other side was uneven welding
Why 3 Gap of Joint is over size
Why 4 Gap not maintained during rounding
Why 5 Error in Rounding operation
Root Cause (Occurance) 1-Gap of Joint is over size 2-Error in Rounding operation
 
Root Cause Analysis (Outflow)
Why 1 Defective part passed at customer end
Why 2 Defective part not detected by inspector
Why 3 Inspector was not followed the WI
Why 4
Why 5
Root Cause (Outflow) Defective part not detected by inspector
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow200% inspection startedNice Steel Ind.31/07/202401/08/2024Completed
OccuranceDie design changed and now Gap to be provided in tapper in dieNice Steel01/08/202401/08/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 200% visual inspection started
Inspection Method Other
Other Inspection Method 200%
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 200%
10. Evidance of Countermeasure
Occurance (Before) Tool design
980_Occurance_Before.png
Occurance (After) Tool design
980_Occurance_After.png
Outflow (Before) NO DOCUMENT
980_Outflow_Before.png
Outflow (After) OPL
980_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NOT APPLICABLE
 
12. Document Review
Documents WISOP
Specify Other Document OPL
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission still we are receiving the welding issues