QFR No - 8000886626
Defect Details
NC No. 8000886626
NC Date 12/08/2024
NC Submission Date
Part No. 520DZ01203
Part Name FORK BOLT NiCr PLATED ELIMIN.
Supplier Name & Code 101263-SINGLA PRECISION SCREWS
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details THREADING MISSING-WITHOUT THREADING
 
1. Problem Description
Defect Description Threading Missing
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 1
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@singlaprecision.com
Plant Head/CEO Email ID quality@singlaprecision.com
MD Email ID aditya@singlaprecision.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
2000
0
2000
3000
8000
Check Qty
1000
2000
0
2000
3000
8000
NG Qty
1
0
0
0
0
1
 
Scrap 0
Rework 1
Under Deviation 0
Containment Action
we are checked 100% material lying at various stage
 
3. Process Flow
Process Flow Description
Raw Material +Cutting + Annealing + Forging + CNC Turning + Head Facing + Counter + Buffing + Thread Rolling + Surface Treatment + Final Inspection + Packing
 
4. Process Details
Process / Operation Thread Rolling
Outsource No
Machine / Cell Rolling
Machine / Cell No. Rolling machine -02
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodINSPECTION METHOD NOT EFFECTIVEVALIDATION AND FOUND TRG NOT USE 100%IN MACHINEX
ToolDIE WEAROUTVALIDATION AND FOUND DIE OKO
MachineROLLING MACHINE PM NOT DONE AS PER PLANVALIDATION AND FOUND PM DONEO
ManUNAWARENESS OF OPERATORVALIDATION AND FOUND OPERATOR SKILL LEVEL LOWX
MaterialRM GRADE AND SIZE NOT OKVALIDATION ANF FOUND OKO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size SAMPLING
7. Root Cause Analysis (Occurance)
Why 1 THREADING MISSING-WITHOUT THREADING
Why 2 The part skipped the threading process during production.
Why 3 During Rolling Process 1 piece fell down from output bin
Why 4 input and output material separate rack not provide in machine
Why 5 material handling W.I not display on machine and operator training not given input and output material
Root Cause (Occurance) input and output material separate rack not provide in machine input output material bin not different use not add point W.I
 
Root Cause Analysis (Outflow)
Why 1 THREADING MISSING-WITHOUT THREADING
Why 2 The part skipped the Final Inspection during part inspection
Why 3 NG PART SKIPPED FROM INSPECTION
Why 4 Final inspection area Red Bin Lock and key not available
Why 5
Root Cause (Outflow) Final inspection area rejection box lock and key not available
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceInput and output material separate rack provide in machineMr Anil14/08/202414/08/2024Completed
Outflowprovide All inspection table rejection bin lock and keyMr Ganesh Maurya14/08/202414/08/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% THREADING CHECKED IN MACHINE AND FINAL INSPECTION
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) input and output material separate rack not provide in machine input output material bin not different use not add point W.I
1017_Occurance_Before.xlsx
Occurance (After) input and output material separate rack provide in machine and input material blue and output material green bin use add point W.I
1017_Occurance_After.xlsx
Outflow (Before) Final inspection area rejection box lock and key not available
1017_Outflow_Before.xlsx
Outflow (After) Final inspection area rejection box lock and key available
1017_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant ROOLING MACHINE -01
 
12. Document Review
Documents PFMEA, WISOP, PackingStd
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity 50
Reason for submission OK