QFR No - 8000886626
Defect Details
NC No. | 8000886626 |
NC Date | 12/08/2024 |
NC Submission Date | |
Part No. | 520DZ01203 |
Part Name | FORK BOLT NiCr PLATED ELIMIN. |
Supplier Name & Code | 101263-SINGLA PRECISION SCREWS |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | THREADING MISSING-WITHOUT THREADING |
1. Problem Description
Defect Description | Threading Missing |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 1 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@singlaprecision.com |
Plant Head/CEO Email ID | quality@singlaprecision.com |
MD Email ID | aditya@singlaprecision.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1000
|
2000
|
0
|
2000
|
3000
|
8000
|
Check Qty |
1000
|
2000
|
0
|
2000
|
3000
|
8000
|
NG Qty |
1
|
0
|
0
|
0
|
0
|
1
|
Scrap | 0 |
Rework | 1 |
Under Deviation | 0 |
Containment Action |
---|
we are checked 100% material lying at various stage |
3. Process Flow
Process Flow Description |
---|
Raw Material +Cutting + Annealing + Forging + CNC Turning + Head Facing + Counter + Buffing + Thread Rolling + Surface Treatment + Final Inspection + Packing |
4. Process Details
Process / Operation | Thread Rolling |
Outsource | No |
Machine / Cell | Rolling |
Machine / Cell No. | Rolling machine -02 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | INSPECTION METHOD NOT EFFECTIVE | VALIDATION AND FOUND TRG NOT USE 100%IN MACHINE | X |
Tool | DIE WEAROUT | VALIDATION AND FOUND DIE OK | O |
Machine | ROLLING MACHINE PM NOT DONE AS PER PLAN | VALIDATION AND FOUND PM DONE | O |
Man | UNAWARENESS OF OPERATOR | VALIDATION AND FOUND OPERATOR SKILL LEVEL LOW | X |
Material | RM GRADE AND SIZE NOT OK | VALIDATION ANF FOUND OK | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | No |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | SAMPLING |
7. Root Cause Analysis (Occurance)
Why 1 | THREADING MISSING-WITHOUT THREADING |
Why 2 | The part skipped the threading process during production. |
Why 3 | During Rolling Process 1 piece fell down from output bin |
Why 4 | input and output material separate rack not provide in machine |
Why 5 | material handling W.I not display on machine and operator training not given input and output material |
Root Cause (Occurance) | input and output material separate rack not provide in machine input output material bin not different use not add point W.I |
Root Cause Analysis (Outflow)
Why 1 | THREADING MISSING-WITHOUT THREADING |
Why 2 | The part skipped the Final Inspection during part inspection |
Why 3 | NG PART SKIPPED FROM INSPECTION |
Why 4 | Final inspection area Red Bin Lock and key not available |
Why 5 | |
Root Cause (Outflow) | Final inspection area rejection box lock and key not available |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Input and output material separate rack provide in machine | Mr Anil | 14/08/2024 | 14/08/2024 | Completed |
Outflow | provide All inspection table rejection bin lock and key | Mr Ganesh Maurya | 14/08/2024 | 14/08/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% THREADING CHECKED IN MACHINE AND FINAL INSPECTION |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
input and output material separate rack not provide in machine input output material bin not different use not add point W.I 1017_Occurance_Before.xlsx |
Occurance (After) |
input and output material separate rack provide in machine and input material blue and output material green bin use add point W.I 1017_Occurance_After.xlsx |
Outflow (Before) |
Final inspection area rejection box lock and key not available 1017_Outflow_Before.xlsx |
Outflow (After) |
Final inspection area rejection box lock and key available 1017_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | ROOLING MACHINE -01 |
12. Document Review
Documents | PFMEA, WISOP, PackingStd |
Specify Other Document | NO |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | OK |