QFR No - 8000886627
Defect Details
NC No. 8000886627
NC Date 12/08/2024
NC Submission Date
Part No. F2LG05402B
Part Name SEAT PIPE - J1A & J1D
Supplier Name & Code 101263-SINGLA PRECISION SCREWS
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-MIX-UP
 
1. Problem Description
Defect Description Mix-up Issue
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 37
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@singlaprecision.com
Plant Head/CEO Email ID quality@singlaprecision.com
MD Email ID aditya@singlaprecision.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2000
3000
0
5000
5000
15000
Check Qty
2000
3000
0
5000
5000
15000
NG Qty
37
0
0
0
0
37
 
Scrap 0
Rework 37
Under Deviation 0
Containment Action
STOCK CHECK 100% AT OUR END
 
3. Process Flow
Process Flow Description
1-RM 2- FORGING 3-PUNCHING -IST 4-ROUGH CLG 5-CNC-IST 6-CNC-II 7-PUNCHING -II 8-I.D CHIP REMOVE 9-REAMING IST 10-REAMING-IIND 11- TAPPING 12-FINAL GRINDING 13-ALKLINE WASHING 14- FINAL INSPECTION 15 - PACKING
 
4. Process Details
Process / Operation Packing
Outsource No
Machine / Cell no
Machine / Cell No. no
5. Problem Analysis
Type Possible Cause Fact Verification Jud
Machinematerial mix-up machine stagevalidation and found okO
ManUNAWARENESS OF OPERATORVALIDATION AND FOUND MACHINE OPERATOR AWARENESS FOR J1A & J1D MATERIAL HANDLINGO
MethodPACKING STANDARDS NOT EFFECTIVEVALIDATION FOUND MATERIAL MIX-UP FOR PACKING STAGEX
MaterialRM GRADE AND SIZE NOT OKVALIDATED AND FOUND OK OO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method PACKING OTHERS STAGE
Check Point at Final Inspection No
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 NOT AS PER SPECIFICATION-MIX-UP
Why 2 The problem occurred at packing stage
Why 3 Material handling not properly rust preventive oil stage
Why 4 Rust preventive oil stage as per part wise specification bin not use so parts mix-up at this stage
Why 5 No any quality gate available after rust preventive oil material handling
Root Cause (Occurance) No any quality gate available after rust preventive oil stage W I not update as per part wise specification bin
 
Root Cause Analysis (Outflow)
Why 1 NOT AS PER SPECIFICATION-MIX-UP
Why 2 100% inspection is not done at packing stage
Why 3 Inspection is also as per sampling plan
Why 4 So final inspection person not caught this defect
Why 5 So NG parts dispatched to customer end
Root Cause (Outflow) Seat pipe J1D material identification groove require as per process drg. same implement but at packing stage this point not highlight in packing std.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occuranceprepared quality gate and W I update point after rust preventive oil stage same specification bin use for input /output materialAnil14/08/202414/08/2024Completed
Outflowpacking std. change and highlight groove identification mark and all packging opr. training provideGanesh mourya14/08/202414/08/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details AFTER MATERIAL INSPECTION SOME TABLE PACKING DONE
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) No any quality gate available after rust preventive oil stage W I not update as per part wise specification bin
1019_Occurance_Before.pdf
Occurance (After) quality gate available after rust preventive oil stage W I update as per part wise specification bin
1019_Occurance_After.pdf
Outflow (Before) PACKING STANDARDS NOT UPDATE AS PER PART WISE IDENTIFICATION MARK
1019_Outflow_Before.pdf
Outflow (After) PACKING STANDARDS UPDATE AS PER PART WISE IDENDITFICATION MARK
1019_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant J1A ~ J1D MODLE
 
12. Document Review
Documents ControlPlan, PFMEA, PackingStd
Specify Other Document OPL
 
13. Effectiveness Of Action
Reviewed Quantity 50
Reason for submission Occurrence side action plan?