QFR No - 8000886627
Defect Details
NC No. | 8000886627 |
NC Date | 12/08/2024 |
NC Submission Date | |
Part No. | F2LG05402B |
Part Name | SEAT PIPE - J1A & J1D |
Supplier Name & Code | 101263-SINGLA PRECISION SCREWS |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-MIX-UP |
1. Problem Description
Defect Description | Mix-up Issue |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 37 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@singlaprecision.com |
Plant Head/CEO Email ID | quality@singlaprecision.com |
MD Email ID | aditya@singlaprecision.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
2000
|
3000
|
0
|
5000
|
5000
|
15000
|
Check Qty |
2000
|
3000
|
0
|
5000
|
5000
|
15000
|
NG Qty |
37
|
0
|
0
|
0
|
0
|
37
|
Scrap | 0 |
Rework | 37 |
Under Deviation | 0 |
Containment Action |
---|
STOCK CHECK 100% AT OUR END |
3. Process Flow
Process Flow Description |
---|
1-RM 2- FORGING 3-PUNCHING -IST 4-ROUGH CLG 5-CNC-IST 6-CNC-II 7-PUNCHING -II 8-I.D CHIP REMOVE 9-REAMING IST 10-REAMING-IIND 11- TAPPING 12-FINAL GRINDING 13-ALKLINE WASHING 14- FINAL INSPECTION 15 - PACKING |
4. Process Details
Process / Operation | Packing |
Outsource | No |
Machine / Cell | no |
Machine / Cell No. | no |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | material mix-up machine stage | validation and found ok | O |
Man | UNAWARENESS OF OPERATOR | VALIDATION AND FOUND MACHINE OPERATOR AWARENESS FOR J1A & J1D MATERIAL HANDLING | O |
Method | PACKING STANDARDS NOT EFFECTIVE | VALIDATION FOUND MATERIAL MIX-UP FOR PACKING STAGE | X |
Material | RM GRADE AND SIZE NOT OK | VALIDATED AND FOUND OK O | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | PACKING OTHERS STAGE |
Check Point at Final Inspection | No |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | NOT AS PER SPECIFICATION-MIX-UP |
Why 2 | The problem occurred at packing stage |
Why 3 | Material handling not properly rust preventive oil stage |
Why 4 | Rust preventive oil stage as per part wise specification bin not use so parts mix-up at this stage |
Why 5 | No any quality gate available after rust preventive oil material handling |
Root Cause (Occurance) | No any quality gate available after rust preventive oil stage W I not update as per part wise specification bin |
Root Cause Analysis (Outflow)
Why 1 | NOT AS PER SPECIFICATION-MIX-UP |
Why 2 | 100% inspection is not done at packing stage |
Why 3 | Inspection is also as per sampling plan |
Why 4 | So final inspection person not caught this defect |
Why 5 | So NG parts dispatched to customer end |
Root Cause (Outflow) | Seat pipe J1D material identification groove require as per process drg. same implement but at packing stage this point not highlight in packing std. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | prepared quality gate and W I update point after rust preventive oil stage same specification bin use for input /output material | Anil | 14/08/2024 | 14/08/2024 | Completed |
Outflow | packing std. change and highlight groove identification mark and all packging opr. training provide | Ganesh mourya | 14/08/2024 | 14/08/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | AFTER MATERIAL INSPECTION SOME TABLE PACKING DONE |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
No any quality gate available after rust preventive oil stage W I not update as per part wise specification bin 1019_Occurance_Before.pdf |
Occurance (After) |
quality gate available after rust preventive oil stage W I update as per part wise specification bin 1019_Occurance_After.pdf |
Outflow (Before) |
PACKING STANDARDS NOT UPDATE AS PER PART WISE IDENTIFICATION MARK 1019_Outflow_Before.pdf |
Outflow (After) |
PACKING STANDARDS UPDATE AS PER PART WISE IDENDITFICATION MARK 1019_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | J1A ~ J1D MODLE |
12. Document Review
Documents | ControlPlan, PFMEA, PackingStd |
Specify Other Document | OPL |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | Occurrence side action plan? |