QFR No - 8000886629
Defect Details
NC No. | 8000886629 |
NC Date | 12/08/2024 |
NC Submission Date | |
Part No. | F2DZ04603B |
Part Name | FORK BOLT J1A & J1D |
Supplier Name & Code | 100106-SHARP ENGINEERS. |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-FORGING DENT |
1. Problem Description
Defect Description | FORGING DENT |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 1 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@sharp-engineers.com |
Plant Head/CEO Email ID | kurund.ma@sharp-engineers.com |
MD Email ID | urkhandelwal@sharp-engineers.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
400
|
0
|
0
|
300
|
0
|
700
|
Check Qty |
400
|
0
|
0
|
300
|
0
|
700
|
NG Qty |
1
|
0
|
0
|
0
|
0
|
1
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Segregated all pipeline material at ETL end and Sharp end |
3. Process Flow
Process Flow Description |
---|
RM incoming-Parting and drilling-Milling-CNC 1st-Deburring-CNC 2nd-Finish Drilling--Tapping-Plating-Final Inspection-PDIR-Packing and forwarding |
4. Process Details
Process / Operation | RM incoming |
Outsource | Yes |
Machine / Cell | NA |
Machine / Cell No. | NA |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Part not clamp properly | Clamping done properly | O |
Tool | Tool make grade change | Tool found as per specification | O |
Material | Hardness variation | Found ok | O |
Material | Material in damage condition | One bar found in damage condition in same lot | X |
Man | Unskill manpower | Skill manpower deployed | O |
Material | Material Grade change | Grade found ok | O |
Method | SOP not followed | SOP available on stage | O |
Method | Fixture Not clean Properly | Fixture found clean | O |
Man | Manpower change | Manpower deployed ase per skill matrix | O |
Tool | Tool not change at defined frequency | Change at defined frequency | O |
Man | Inspector Change | Inspector change coz regular inspector in on leave for one day | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 nos per |
7. Root Cause Analysis (Occurance)
Why 1 | Deep Line mark |
Why 2 | Deep line mark on collar |
Why 3 | Deep line mark on RM |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Deep line mark on RM |
Root Cause Analysis (Outflow)
Why 1 | Deep Line mark |
Why 2 | skip from inspection |
Why 3 | Inspector changed |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Inspector changed |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | started 100% inspection at supplier end with white colour identification mark and same verification at Incoming Stage | Yogesh Chavan | 22/08/2024 | 22/08/2024 | Completed |
Outflow | on job training given to inspector also, started inspector initials tag along with bins | Omkar Bhange | 20/08/2024 | 20/08/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | RM verification started at incoming stage. |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
5 nos bar per lot 1021_Occurance_Before.jpeg |
Occurance (After) |
100% checking started with white colour identification before dispatch at supplier end also verification at incoming stage. 1021_Occurance_After.jpeg |
Outflow (Before) |
100% inspection but without inspectors tag 1021_Outflow_Before.jpeg |
Outflow (After) |
on job training given to inspector also, started inspector initials tag along with bins 1021_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NA |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP |
Specify Other Document | NA |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | Occurrence side route cause can do better and action only inspection is not sufficient need preventive action to avoid re-occurrence. Outflow side inspector change is related to 4M which is not addressed in 4M analysis and also not declared about 4M change |