QFR No - 8000887123
Defect Details
NC No. | 8000887123 |
NC Date | 16/08/2024 |
NC Submission Date | |
Part No. | F2DZ04603B |
Part Name | FORK BOLT J1A & J1D |
Supplier Name & Code | 100106-SHARP ENGINEERS. |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-BIN CONTAMINATION |
1. Problem Description
Defect Description | BIN CONTAMINATION |
Detection Stage | Receipt |
Problem Severity | Function |
NG Quantity | 528 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@sharp-engineers.com |
Plant Head/CEO Email ID | kurund.ma@sharp-engineers.com |
MD Email ID | urkhandelwal@sharp-engineers.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1000
|
0
|
0
|
0
|
0
|
1000
|
Check Qty |
1000
|
0
|
0
|
0
|
0
|
1000
|
NG Qty |
528
|
0
|
0
|
0
|
0
|
528
|
Scrap | 0 |
Rework | 528 |
Under Deviation | 0 |
Containment Action |
---|
Clean all pipeline material |
3. Process Flow
Process Flow Description |
---|
RM incoming-Parting and drilling-Milling-CNC 1st-Deburring-CNC 2nd-Finish Drilling--Tapping-Plating-Final Inspection-PDIR-Packing and forwarding |
4. Process Details
Process / Operation | Dispatch |
Outsource | No |
Machine / Cell | NA |
Machine / Cell No. | NA |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | New manpower for packaging | Having existing manpower | O |
Tool | Tool change | Not applicable | O |
Machine | Machined change | No machine change | O |
Method | Bin cleaning not done at defined frequency | Bin cleaning not done as per defined frequency | X |
Method | Bin Received in contamination condition from customer | Received in ok condition | O |
Material | Material grade change | Material found ok | O |
Method | other parts Bin used for dispatched | Having Possibilities | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | No |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 nos |
7. Root Cause Analysis (Occurance)
Why 1 | Contamination Bin |
Why 2 | Oil found in Bin |
Why 3 | Used other parts Bin for dispatched |
Why 4 | Shortage of Bins |
Why 5 | |
Root Cause (Occurance) | Shortage of Bins |
Root Cause Analysis (Outflow)
Why 1 | Contamination Bin |
Why 2 | Bin condition not verified at PDI stage |
Why 3 | Check Point not available in PDI report |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Check Point not available in PDI report |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | Check point added in PDI report | Mr. Omkar Bhange | 20/08/2024 | 20/08/2024 | Completed |
Occurance | Ordered New 50nos Bins | Mr. Vivek Dewar | 11/09/2024 | 20/08/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Check point added at PDI stage |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Contamination in Bin 1024_Occurance_Before.png |
Occurance (After) |
Ordered New 50 Nos Bins 1024_Occurance_After.pdf |
Outflow (Before) |
Check point not added in PDI report 1024_Outflow_Before.jpeg |
Outflow (After) |
Check point added in PDI report 1024_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | NA |
12. Document Review
Documents | PFMEA, WISOP, InspCheckSheet |
Specify Other Document | NA |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | OK But preventive action is required |