QFR No - 8000887128
Defect Details
NC No. 8000887128
NC Date 16/08/2024
NC Submission Date
Part No. F2DZ15510B
Part Name FORK BOLT -ACJA FF
Supplier Name & Code 100505-A B AUTOCOMPONENTS
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-COLOUR SHADING
 
1. Problem Description
Defect Description COLOUR SHADING
Detection Stage Customer End
Problem Severity Aesthetic
NG Quantity 9
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID headqaabauto@gmail.com
Plant Head/CEO Email ID kamalabautocomponent@gmail.com
MD Email ID abautocomponent@gmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2000
0
0
0
400
2400
Check Qty
2000
0
0
0
400
2400
NG Qty
9
0
0
0
0
9
 
Scrap 9
Rework 0
Under Deviation 0
Containment Action
Verify the WIP stocks, there is no FG qty.
 
3. Process Flow
Process Flow Description
CNC Turning >VMC Milling >Special process.
 
4. Process Details
Process / Operation Turning, Milling & Black Anodizing
Outsource Yes
Machine / Cell CNC & VMC & Special process
Machine / Cell No. CNC & VMC & Special
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolPart clamp issueVerified Jig problem found.X
ManPart Jigging variationVerified found okO
MethodProcess variationProcess parameters witnessed and found ok.O
MachineMaintenance overdue.Preventive Maintenance verification done, found okO
MachinePower fluctuationVerified found okO
MaterialChemical usedVerified found okO
MaterialCleaning agentsVerified there is no cleaning agent using.O
MethodCleaning problemThere is no cleaning required with agent, Only cloth cleaning found ok.O
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Limit sample visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Shade variation.
Why 2 Due to the Part hold in the jig, improper hold / part shake will create the shade variation in the part.
Why 3 Part holding not rigid in the jigs.
Why 4 Jigs weaker
Why 5 Jigs Life does not monitor.
Root Cause (Occurance) Due to the Part hold in the jig, improper hold / part shake will create the shade variation in the part.
 
Root Cause Analysis (Outflow)
Why 1 Shade variation
Why 2 Not witnessed during final visual inspection.
Why 3 Due to shade variation not capturing immediately.
Why 4 Shade generation will take time to appear.
Why 5
Root Cause (Outflow) Shade generation will take time to appear.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceMonitor the Jig life through number of Batch processed, also verify the jigs while loading the part. SIR report updated, also revise the supplier inspection reports.Karan Metals04/09/202402/09/2024Completed
OutflowAvoid the immediate dispatches from AB Auto to ETL to avid shade issues.Rudresh04/09/202402/09/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100 % visual after one-week FG WIP Stock.
Inspection Method Other
Other Inspection Method WIP stock maintain
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Monthly verifying the Anodizing processes through check list.
1026_Occurance_Before.pdf
Occurance (After) Anodizing process verifying each batch by updating the checklist.
1026_Occurance_After.pdf
Outflow (Before) Same day dispatch after anodizing
1026_Outflow_Before.pdf
Outflow (After) Minimum one week kept before dispatch after FG.
1026_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Fork bolts & screw caps.
 
12. Document Review
Documents AuditCheckSheet, InspCheckSheet
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 50
Reason for submission 05 Problem analysis - Fact verification need to correct as per actual observation against 4M and give judgment `X` for not ok and `O` for OK