QFR No - 8000887715
Defect Details
NC No. 8000887715
NC Date 20/08/2024
NC Submission Date
Part No. 52GQ01013O
Part Name M/CYL BODY PDC BORE BURNISHED -K11,K2,
Supplier Name & Code 101100-CAST 4 ALUMINIUM PVT LTD
ETL Plant 1120-ETL K-226/2 Disc Brakes
Defect Details BLOW HOLES-BH AFTER MACHINING
 
1. Problem Description
Defect Description BLOW HOLES-BH AFTER MACHINING
Detection Stage Inprocess
Problem Severity Function
NG Quantity 58
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID info@cast4aluminium.com
Plant Head/CEO Email ID info@cast4aluminium.com
MD Email ID kiran@cast4aluminium.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
0
0
0
456
1456
Check Qty
1000
0
0
0
456
1456
NG Qty
695
0
0
0
103
798
 
Scrap 695
Rework 0
Under Deviation 0
Containment Action
Not ok parts rejected and scrapped.
 
3. Process Flow
Process Flow Description
RM inward & inspection -- melting -- N2 degassing -- PDC -- gate cutting -- inspection -- fettling -- shot blasting -- inspection -- packing & dispatch
 
4. Process Details
Process / Operation PDC
Outsource No
Machine / Cell PDC machine
Machine / Cell No. PDC machine no. 8
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodMaterial cleaning freq. not adequatenoO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Blow hole observed in bore of master cylinder.
Why 2 Impurities observed in material.
Why 3 material cleaning freq. was decided but not effective.
Why 4
Why 5
Root Cause (Occurance) material cleaning freq. was decided but not effective.
 
Root Cause Analysis (Outflow)
Why 1 Blow hole observed in bore of master cylinder.
Why 2 New inspector was working on boroscope inspection.
Why 3 Understanding of defects was less in inspector.
Why 4
Why 5
Root Cause (Outflow) Understanding of defects was less in inspector.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceMaterial cleaning freq. revised i.e. thrice in a shift.Mubarak27/08/202427/08/2024Completed
OutflowTraining given to inspector regarding understanding of defects.Mahesh G.27/08/202427/08/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details Na
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) NA
1034_Occurance_Before.pdf
Occurance (After) Cleaning freq. decided thrice in a shift and updated in CP.
1034_Occurance_After.pdf
Outflow (Before) NA
1034_Outflow_Before.png
Outflow (After) Awareness given to inspector.
1034_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All master cylinders
 
12. Document Review
Documents ControlPlan, InspCheckSheet
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 200
Reason for submission No blow hole found in 200 Nos lot.