QFR No - 8000889489
Defect Details
NC No. 8000889489
NC Date 02/09/2024
NC Submission Date
Part No. F2AV00302B
Part Name BELLOW-B104B
Supplier Name & Code 101023-FORES ELASTOMECH INDIA PVT. LT
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-CUT MARK
 
1. Problem Description
Defect Description CUT MARK
Detection Stage Inprocess
Problem Severity Aesthetic
NG Quantity 9
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID malani.pritam@foresgroup.com
Plant Head/CEO Email ID singh.barinder@foresgroup.com
MD Email ID swamy.pj@foresgroup.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
0
0
1000
0
2000
Check Qty
1000
0
0
1000
0
2000
NG Qty
9
0
0
0
0
9
 
Scrap 9
Rework 0
Under Deviation 0
Containment Action
Sorting all stock
 
3. Process Flow
Process Flow Description
Rm inward - Mixing - Moulding -Final Inspection.
 
4. Process Details
Process / Operation Moulding
Outsource No
Machine / Cell Cell
Machine / Cell No. cell number 2
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialVerification of Compound as per control plan.Found match with control plan & production report. Checked one month data & found okayO
ToolLess material flow in cavityLeakage in mould cavityX
MachineProcess parameter of moulding not followedFound matched with control plan & automatic PLC controlO
MethodMix up during packingoffline packingX
ManUn skill InspectorSkill level verified found L3 & Required L3O
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Flow mark
Why 2 Less material flow in cavity
Why 3 leakage in mould cavity.
Why 4 Mould plate parallelism not okay
Why 5
Root Cause (Occurance) Mould plate parallelism not okay
 
Root Cause Analysis (Outflow)
Why 1 Flow mark
Why 2 Skipped from Fores quality
Why 3 Not checked part mixed in okay part after quality inspection
Why 4 Offline box packing
Why 5
Root Cause (Outflow) Offline box packing
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow`Online packing implementedPande25/08/202415/07/2024Completed
OccuranceMould leakage removed by making plate parallelism okay.Ravi11/07/202426/06/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details NA
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Mould parallelism not okay
1056_Occurance_Before.pdf
Occurance (After) Mould parallelism okay
1056_Occurance_After.pdf
Outflow (Before) Offline packing
1056_Outflow_Before.pdf
Outflow (After) Online packing
1056_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Cell no 1
 
12. Document Review
Documents
Specify Other Document OPL
 
13. Effectiveness Of Action
Reviewed Quantity 50
Reason for submission ok