QFR No - 8000889501
Defect Details
NC No. 8000889501
NC Date 02/09/2024
NC Submission Date
Part No. F2DZ07203B
Part Name FORK BOLT (K-9207) Ni+Cr Plated
Supplier Name & Code 100539-N P ENTERPRISES
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-RUSTY
 
1. Problem Description
Defect Description RUSTY
Detection Stage Inprocess
Problem Severity Aesthetic
NG Quantity 3
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@npcindustries.in
Plant Head/CEO Email ID anand@npcindustries.in
MD Email ID ajay@npcindustries.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1008
375
1000
0
0
2383
Check Qty
1008
375
1000
0
0
2383
NG Qty
3
2
0
0
0
5
 
Scrap 5
Rework 0
Under Deviation 0
Containment Action
1-Raw Material Receipt 2- Cutting & Forging 1st 3-Annealing 4-Phosphating 5-Forging - 2nd 6-CNC1st 7-CNC 2nd 8-Thread Rolling 9-Drilling 10-Buffing 11-Head Polishing 12-Plating 13-Final Inspection 14-Packing & Dispatch
 
3. Process Flow
Process Flow Description
Plating
 
4. Process Details
Process / Operation Plating process
Outsource Yes
Machine / Cell Plating setup
Machine / Cell No. plating tank
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManPlating operator negligentOperator found to be not negligentO
ManOperator unaware about processOperator found to be aware about the processO
MethodIncoming material for plating rustyIncoming material for plating observed to be rustyX
MaterialRPO not applied uniformly on all partsUneven application of RPO found during inspectionX
MaterialMaterial not as per drawingMaterial observed as per drawingO
MethodNG part could not be detected at final inspectionIt was observed that NG part skipped final inspectionX
MethodHigh humidity in storage area leading to rust formationStorage environment found to have high humidity levelsO
MachineBuffing machine calibration was incorrectMachine calibration found to be correctO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Bolt caps found rusty at the customer’s end
Why 2 The bolt caps were received with rust before plating.
Why 3 The rust preventive oil (RPO) was not present on the material during the plating process.
Why 4 There were inconsistencies in the method or coverage of RPO application and rpo dipping time less.
Why 5 The standard operating procedure (SOP)/WI for RPO application was not detailed enough.
Root Cause (Occurance) The standard operating procedure (SOP) for RPO application was either not detailed enough .
 
Root Cause Analysis (Outflow)
Why 1 Bolt caps found rusty at the customer’s end
Why 2 Rust was not identified during the final inspection process.
Why 3 The inspector missed detecting rust on the parts.
Why 4 The inspector did not differentiate between rusted parts and acceptable parts.
Why 5 The rust was in its initial phase and not easily detectable through normal visual inspection methods.
Root Cause (Outflow) The rust was in its initial phase and not easily detectable through normal visual inspection methods.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowProvide training to inspectors on identifying early-stage rust, Including visual cues and distinguishing features between rust and minor surface defects.Mr. Deepak05/09/202405/09/2024Completed
OccuranceQ-Alert to be displayed at ROP Station.Mr. Rakesh Thakur05/09/202402/09/2024Completed
OccuranceA detailed SOP should be established for the RPO application process, ensuring complete coverage of the bolt cap and incress the RPO dipping time of bolt.Mr. Rakesh Thakur08/09/202407/09/2024Completed
OutflowQ-Alert to be displayed at final inspection.Mr. Princ04/09/202403/09/2024Completed
OutflowAwareness should be raised among inspection teams about the importance of identifying early stage corrosion and its impact on product quality.Mr. Deepak05/09/202404/09/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details Awareness should be raised among inspection teams about the importance of identifying early stage corrosion and its impact on product quality.
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) No Special training was given to inspectors for early-stage rust detection.
1057_Occurance_Before.png
Occurance (After) Provide training to inspectors on identifying early-stage rust, Including visual cues and distinguishing features between rust and minor surface defects.
1057_Occurance_After.jpg
Outflow (Before) There were inconsistencies in the method or coverage of RPO application and RPO dipping time less.
1057_Outflow_Before.jpg
Outflow (After) RPO Dipping time increased and WI to be updated.
1057_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Similar Models
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP, PackingStd, InspCheckSheet
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 50
Reason for submission OK