QFR No - 8000889502
Defect Details
NC No. | 8000889502 |
NC Date | 02/09/2024 |
NC Submission Date | |
Part No. | 550PH00412 |
Part Name | VALVE RETAINER |
Supplier Name & Code | 101255-MAHAVIR INDUSTRIES |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-CUT MARK |
1. Problem Description
Defect Description | Grinding damage |
Detection Stage | Inprocess |
Problem Severity | Function |
NG Quantity | 3 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@mahavirind.co.in |
Plant Head/CEO Email ID | planthead@mahavirind.co.in |
MD Email ID |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
750
|
0
|
0
|
0
|
1800
|
2550
|
Check Qty |
750
|
0
|
0
|
0
|
1800
|
2550
|
NG Qty |
3
|
0
|
0
|
0
|
0
|
3
|
Scrap | 3 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All Suspected Material Segregation at Customer End |
3. Process Flow
Process Flow Description |
---|
RM Inward - Store- Parting on Traub Machine - CNC counter boring and facing - OD Grinding- plating-- Final Inspection - Dispatch |
4. Process Details
Process / Operation | OD Grinding |
Outsource | No |
Machine / Cell | CLG Grinding Section |
Machine / Cell No. | CLG-5 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Process &Inspection Method Wrong | Process Method Ok But Inspection Method After OD Grinding visual frequency Very Low | X |
Man | Unskilled operator | As per Skilled Matrix Operator is Skilled | O |
Material | Hard And other grade Material Use | Hardness 80-94 HRB and as per required grade CEW-3 Material Use. | O |
Tool | Wrong Grinding Wheel Use and work Rest blade | As Per Store Record Ok CUMI Make Grinding Wheel Use.But Work Rest Blade Thickness Not Ok | X |
Machine | Machine Condition Not oK or RPM over | Machine Condition ok But Control Wheel RPM was 35--45 | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | NOT AS PER SPECIFICATION-CUT MARK |
Why 2 | As per part diameter size Work Rest Blade Not use |
Why 3 | Part Damage During part feeding on OD Grinding Process. |
Why 4 | Part Not Proper Rest on work rest blade during OD Grinding process On Grinding Machine |
Why 5 | Work Rest Blade Thickness was Under size Instead of Required Thickness . |
Root Cause (Occurance) | Work Rest Blade Thickness was Under size |
Root Cause Analysis (Outflow)
Why 1 | NOT AS PER SPECIFICATION-CUT MARK |
Why 2 | Final Inspection stage Not Detect During Visual sampling Inspection |
Why 3 | After OD Grinding Process & Final Inspection stage visual frequency Very Low |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | After OD Grinding Process & Final Inspection stage visual frequency Very Low |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | Sampling Frequency Increase 100% per 500nos Bag Instead Of 20/500nos& After Visual Inspection Tick Marks On OD at Final Stage. | Quality Head | 20/09/2024 | 21/09/2024 | Completed |
Occurance | Work Rest blade Thickness Increase 20insted Of 10mm | Production Head | 04/10/2024 | 03/10/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Previously, the price was 20 nos per bag; now it is 100% per bag. Inspection |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Work Rest Blade Thickness was Under size 1059_Occurance_Before.jpg |
Occurance (After) |
Work Rest blade Thickness Increase 20mm instead of 10mm 1059_Occurance_After.jpg |
Outflow (Before) |
After OD Grinding Process & Final Inspection stage visual frequency Very Low 1059_Outflow_Before.docx |
Outflow (After) |
Sampling Frequency Increase 100% per 500nos Bag Instead Of 20/500nos& After Visual Inspection Tick Marks On OD at Final Stage. 1059_Outflow_After.docx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All Valve Retainers models |
12. Document Review
Documents | ControlPlan, PFMEA, InspCheckSheet |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | OK |