QFR No - 8000889502
Defect Details
NC No. 8000889502
NC Date 02/09/2024
NC Submission Date
Part No. 550PH00412
Part Name VALVE RETAINER
Supplier Name & Code 101255-MAHAVIR INDUSTRIES
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-CUT MARK
 
1. Problem Description
Defect Description Grinding damage
Detection Stage Inprocess
Problem Severity Function
NG Quantity 3
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@mahavirind.co.in
Plant Head/CEO Email ID planthead@mahavirind.co.in
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
750
0
0
0
1800
2550
Check Qty
750
0
0
0
1800
2550
NG Qty
3
0
0
0
0
3
 
Scrap 3
Rework 0
Under Deviation 0
Containment Action
All Suspected Material Segregation at Customer End
 
3. Process Flow
Process Flow Description
RM Inward - Store- Parting on Traub Machine - CNC counter boring and facing - OD Grinding- plating-- Final Inspection - Dispatch
 
4. Process Details
Process / Operation OD Grinding
Outsource No
Machine / Cell CLG Grinding Section
Machine / Cell No. CLG-5
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodProcess &Inspection Method WrongProcess Method Ok But Inspection Method After OD Grinding visual frequency Very LowX
ManUnskilled operatorAs per Skilled Matrix Operator is SkilledO
MaterialHard And other grade Material UseHardness 80-94 HRB and as per required grade CEW-3 Material Use.O
ToolWrong Grinding Wheel Use and work Rest bladeAs Per Store Record Ok CUMI Make Grinding Wheel Use.But Work Rest Blade Thickness Not OkX
MachineMachine Condition Not oK or RPM overMachine Condition ok But Control Wheel RPM was 35--45O
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 NOT AS PER SPECIFICATION-CUT MARK
Why 2 As per part diameter size Work Rest Blade Not use
Why 3 Part Damage During part feeding on OD Grinding Process.
Why 4 Part Not Proper Rest on work rest blade during OD Grinding process On Grinding Machine
Why 5 Work Rest Blade Thickness was Under size Instead of Required Thickness .
Root Cause (Occurance) Work Rest Blade Thickness was Under size
 
Root Cause Analysis (Outflow)
Why 1 NOT AS PER SPECIFICATION-CUT MARK
Why 2 Final Inspection stage Not Detect During Visual sampling Inspection
Why 3 After OD Grinding Process & Final Inspection stage visual frequency Very Low
Why 4
Why 5
Root Cause (Outflow) After OD Grinding Process & Final Inspection stage visual frequency Very Low
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowSampling Frequency Increase 100% per 500nos Bag Instead Of 20/500nos& After Visual Inspection Tick Marks On OD at Final Stage.Quality Head20/09/202421/09/2024Completed
OccuranceWork Rest blade Thickness Increase 20insted Of 10mmProduction Head04/10/202403/10/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Previously, the price was 20 nos per bag; now it is 100% per bag. Inspection
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Work Rest Blade Thickness was Under size
1059_Occurance_Before.jpg
Occurance (After) Work Rest blade Thickness Increase 20mm instead of 10mm
1059_Occurance_After.jpg
Outflow (Before) After OD Grinding Process & Final Inspection stage visual frequency Very Low
1059_Outflow_Before.docx
Outflow (After) Sampling Frequency Increase 100% per 500nos Bag Instead Of 20/500nos& After Visual Inspection Tick Marks On OD at Final Stage.
1059_Outflow_After.docx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Valve Retainers models
 
12. Document Review
Documents ControlPlan, PFMEA, InspCheckSheet
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 50
Reason for submission OK