QFR No - 8000890615
Defect Details
NC No. 8000890615
NC Date 10/09/2024
NC Submission Date
Part No. 550LG06202
Part Name SEAT PIPE -K23A/PRFH-006
Supplier Name & Code 100538-NARINDER PARKASH AND CO
ETL Plant 1146-ETL Suspension Narasapura
Defect Details MIX UP OTHER MODEL-NOT USING KON MODEL
 
1. Problem Description
Defect Description Wrong seat pipe received not using kONF front fork model
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 100
Is Defect Repeatative? No
Defect Sketch / Photo mmuyicwg5a5ntybia1zkifgc.jpg
Supplier Communication Details
Quality Head Email ID quality@npcindustries.in
Plant Head/CEO Email ID anand@npcindustries.in
MD Email ID ajay@npcindustries.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
10000
0
4500
5000
5000
24500
Check Qty
10000
0
4500
5000
5000
24500
NG Qty
100
0
0
0
0
100
 
Scrap 0
Rework 100
Under Deviation 0
Containment Action
100% visual inspection of available material
 
3. Process Flow
Process Flow Description
1.RM Receipt 2. Cutting 3.Multistation Draw 4. Head Formation 5. Punching 6. Rough Grinding 7. CNC Head Turning & Chamfering 8. CNC Boring & Facing 9. Thread M8x1.25 Tapping 10. Chamfering-1 11. Chamfering-2 12. ID Deburring 13. Finish Grinding 14. Final Inspection 15. ID Cleaning 16. Oiling 17. Packing & Dispatch
 
4. Process Details
Process / Operation Packing & Dispatch
Outsource No
Machine / Cell Packing & Dispatch Section
Machine / Cell No. Dispatch
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodMix up at final InspectionNo mix up at final observedO
MethodNo checkpoint for checking Barcode StickersIt was observed no checkpoint available for checking Barcode stickersde StickersX
MethodMix up by transportMix up by transport observedX
ManIn process operator negligent .In process operator was not found to be negligent .O
ManQuality Inspector negligentQuality Inspector was not found to be negligent.O
MethodMix up during PackingAfter verification it was observed that parts were not mixed during PackingO
MethodMaterial identification missingMaterial identification observed to be presentO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Mix up other model
Why 2 Other model box dispatched to Narsapura
Why 3 Wrong sticker got pasted on Packing Bag
Why 4 Sticker gets detached from Bag
Why 5 Sticker pasted on Bag instead of Tag
Root Cause (Occurance) Sticker pasted on Bag instead of paper Tag
 
Root Cause Analysis (Outflow)
Why 1 Mix up other model
Why 2 Wrong sticker got pasted on Packing Bag
Why 3 Could not be detected before dispatch
Why 4 No checkpoint for checking Barcode Stickers by Transport before dispatch
Why 5
Root Cause (Outflow) No checkpoint for checking Barcode Stickers by Transport before dispatch
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceWI to be displayed in Dispatch AreaMr Ankush17/09/202416/09/2024Completed
Outflow100% inspection of Barcode Stickers before dispatch to be doneMr Ankush13/09/202413/09/2024Completed
OutflowQuality Alert to be displayed in Dispatch AreaMr Princ18/09/202414/09/2024Completed
OccuranceBarcode Stickers to be pasted on Tags instead of BagsMr Ankush16/09/202414/09/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Checkpoint of checking Barcode Stickers 100% implemented
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Sticker pasted on Bag instead of paper Tag
1087_Occurance_Before.jpeg
Occurance (After) Barcode Stickers to be pasted on Tags instead of Bags
1087_Occurance_After.jpeg
Outflow (Before) No checkpoint for checking Barcode Stickers by Transport before dispatch.
1087_Outflow_Before.png
Outflow (After) Quality Alert to be displayed in Dispatch Area & 100% inspection of Barcode Stickers before dispatch to be done
1087_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Models
 
12. Document Review
Documents ControlPlan, PMCheckSheet, PFMEA, WISOP, PackingStd, InspCheckSheet
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 40000
Reason for submission reviewed next 3 Lots no mix up issue found ok