QFR No - 8000890615
Defect Details
NC No. | 8000890615 |
NC Date | 10/09/2024 |
NC Submission Date | |
Part No. | 550LG06202 |
Part Name | SEAT PIPE -K23A/PRFH-006 |
Supplier Name & Code | 100538-NARINDER PARKASH AND CO |
ETL Plant | 1146-ETL Suspension Narasapura |
Defect Details | MIX UP OTHER MODEL-NOT USING KON MODEL |
1. Problem Description
Defect Description | Wrong seat pipe received not using kONF front fork model |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 100 |
Is Defect Repeatative? | No |
Defect Sketch / Photo | mmuyicwg5a5ntybia1zkifgc.jpg |
Supplier Communication Details
Quality Head Email ID | quality@npcindustries.in |
Plant Head/CEO Email ID | anand@npcindustries.in |
MD Email ID | ajay@npcindustries.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
10000
|
0
|
4500
|
5000
|
5000
|
24500
|
Check Qty |
10000
|
0
|
4500
|
5000
|
5000
|
24500
|
NG Qty |
100
|
0
|
0
|
0
|
0
|
100
|
Scrap | 0 |
Rework | 100 |
Under Deviation | 0 |
Containment Action |
---|
100% visual inspection of available material |
3. Process Flow
Process Flow Description |
---|
1.RM Receipt 2. Cutting 3.Multistation Draw 4. Head Formation 5. Punching 6. Rough Grinding 7. CNC Head Turning & Chamfering 8. CNC Boring & Facing 9. Thread M8x1.25 Tapping 10. Chamfering-1 11. Chamfering-2 12. ID Deburring 13. Finish Grinding 14. Final Inspection 15. ID Cleaning 16. Oiling 17. Packing & Dispatch |
4. Process Details
Process / Operation | Packing & Dispatch |
Outsource | No |
Machine / Cell | Packing & Dispatch Section |
Machine / Cell No. | Dispatch |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Mix up at final Inspection | No mix up at final observed | O |
Method | No checkpoint for checking Barcode Stickers | It was observed no checkpoint available for checking Barcode stickersde Stickers | X |
Method | Mix up by transport | Mix up by transport observed | X |
Man | In process operator negligent . | In process operator was not found to be negligent . | O |
Man | Quality Inspector negligent | Quality Inspector was not found to be negligent. | O |
Method | Mix up during Packing | After verification it was observed that parts were not mixed during Packing | O |
Method | Material identification missing | Material identification observed to be present | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Mix up other model |
Why 2 | Other model box dispatched to Narsapura |
Why 3 | Wrong sticker got pasted on Packing Bag |
Why 4 | Sticker gets detached from Bag |
Why 5 | Sticker pasted on Bag instead of Tag |
Root Cause (Occurance) | Sticker pasted on Bag instead of paper Tag |
Root Cause Analysis (Outflow)
Why 1 | Mix up other model |
Why 2 | Wrong sticker got pasted on Packing Bag |
Why 3 | Could not be detected before dispatch |
Why 4 | No checkpoint for checking Barcode Stickers by Transport before dispatch |
Why 5 | |
Root Cause (Outflow) | No checkpoint for checking Barcode Stickers by Transport before dispatch |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | WI to be displayed in Dispatch Area | Mr Ankush | 17/09/2024 | 16/09/2024 | Completed |
Outflow | 100% inspection of Barcode Stickers before dispatch to be done | Mr Ankush | 13/09/2024 | 13/09/2024 | Completed |
Outflow | Quality Alert to be displayed in Dispatch Area | Mr Princ | 18/09/2024 | 14/09/2024 | Completed |
Occurance | Barcode Stickers to be pasted on Tags instead of Bags | Mr Ankush | 16/09/2024 | 14/09/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Checkpoint of checking Barcode Stickers 100% implemented |
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Sticker pasted on Bag instead of paper Tag 1087_Occurance_Before.jpeg |
Occurance (After) |
Barcode Stickers to be pasted on Tags instead of Bags 1087_Occurance_After.jpeg |
Outflow (Before) |
No checkpoint for checking Barcode Stickers by Transport before dispatch. 1087_Outflow_Before.png |
Outflow (After) |
Quality Alert to be displayed in Dispatch Area & 100% inspection of Barcode Stickers before dispatch to be done 1087_Outflow_After.png |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All Models |
12. Document Review
Documents | ControlPlan, PMCheckSheet, PFMEA, WISOP, PackingStd, InspCheckSheet |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | 40000 |
Reason for submission | reviewed next 3 Lots no mix up issue found ok |