QFR No - 8000890966
Defect Details
NC No. 8000890966
NC Date 13/09/2024
NC Submission Date
Part No. B2KN01103O
Part Name RESERVOIR CAP RAW CASTING
Supplier Name & Code 100865-HI TECH ARAI PVT LTD UNIT XI
ETL Plant 1120-ETL K-226/2 Disc Brakes
Defect Details BUFFING DEFECT-LETTER MARKING NT OK
 
1. Problem Description
Defect Description BUFFING DEFECT-LETTER MARKING NT OK
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 978
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID rajeshwaran.m@hitecharai.com
Plant Head/CEO Email ID sundararaman.v@hitecharai.com
MD Email ID spm32@hotmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
28000
5000
0
0
3000
36000
Check Qty
28000
5000
0
0
3000
36000
NG Qty
978
200
0
0
0
1178
 
Scrap 1178
Rework 0
Under Deviation 0
Containment Action
ETL End – 978 Qty rejected by ETL . Available stock at Supplier end verified and sorting out.
 
3. Process Flow
Process Flow Description
Casting - fettling
 
4. Process Details
Process / Operation Casting
Outsource No
Machine / Cell Diecasting machice
Machine / Cell No. 125T
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialInsert Chip offInsert verificationO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5 / 2hrs
7. Root Cause Analysis (Occurance)
Why 1 Letter damage issue observed
Why 2 Due to material stuck at letter area
Why 3 Due to insert chip off
Why 4
Why 5
Root Cause (Occurance) Letter damage issue happened due to insert chip off issue.
 
Root Cause Analysis (Outflow)
Why 1 Letter damage issue observed
Why 2 Due to lack of awareness
Why 3 Due to after powder coating only identification
Why 4
Why 5
Root Cause (Outflow) Due to after powder coating only identification
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceInsert send to reformingMr.Balakrishnan05/09/202405/09/2024Completed
OutflowBriefing the quality requirement for fettling operator, inspector & ware house in-charge based on defect details and actual partRajeshwaran / Mane06/09/202406/09/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% inspection on PDI stage
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Defect Photo
1094_Occurance_Before.jpg
Occurance (After) Correction Photo
1094_Occurance_After.jpg
Outflow (Before) No 100% inspection
1094_Outflow_Before.jpg
Outflow (After) To conduct 100% inspection
1094_Outflow_After.jpg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All reservoir Cap
 
12. Document Review
Documents InspCheckSheet
Specify Other Document nil
 
13. Effectiveness Of Action
Reviewed Quantity 150
Reason for submission Improvement found.