QFR No - 8000892985
Defect Details
NC No. 8000892985
NC Date 25/09/2024
NC Submission Date
Part No. F1LG00902B
Part Name SEAT PIPE -K86A
Supplier Name & Code 100538-NARINDER PARKASH AND CO
ETL Plant 1136-ETL Suspension Sanand
Defect Details BROKEN-HEAD SIDE SEAT PIPE BROKEN
 
1. Problem Description
Defect Description Crack from head side
Detection Stage Receipt
Problem Severity Safety
NG Quantity 1
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@npcindustries.in
Plant Head/CEO Email ID anand@npcindustries.in
MD Email ID ajay@npcindustries.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
10000
15000
20000
15000
10000
70000
Check Qty
10000
15000
20000
15000
10000
70000
NG Qty
1
0
0
0
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
100% inspection of available material.
 
3. Process Flow
Process Flow Description
1) Cutting 2) Draw 3) Head Formation 4) Punching 5) Rough Grinding 6) CNC Head Turning 7) CNC Boring & Facing 8) Tapping 9) Chamfering 10) Final Grinding 11) Final Inspection 12) Cleaning 13) Oiling 14) Packing & Dispatch
 
4. Process Details
Process / Operation CNC Head Turning
Outsource No
Machine / Cell CNC
Machine / Cell No. CNC Section
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodHead formation pin depth moreIt was observed that Head Formation Pin Depth is OKO
MethodPart with less wall thickness near groove skipped Final `Q` Gate during inspectionIt was observed that part having less wall thickness near groove skipped Final `Q` GateX
MachineStroke variationNo Stroke variation observedO
MaterialHardness moreMaterial Hardness observed 45HRB which is observed to be within rangeO
MethodSetting part got mixedIt was observed that setting part got mixedX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Head Broken part
Why 2 Crack on part
Why 3 Wall thickness got less
Why 4 Extra machining done
Why 5 Setting part
Root Cause (Occurance) Setting part
 
Root Cause Analysis (Outflow)
Why 1 Head Broken part
Why 2 Could not be detected at final inspection
Why 3 Skipped at Final `Q` Gate
Why 4 Skipped in Groove dia sampling inspection
Why 5 Groove dia sampling qty less
Root Cause (Outflow) Groove dia Sampling Qty less
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow100% inspection of Groove dia to be doneMr Toti02/10/202402/10/2024Completed
OccuranceProper disposal of setting parts to be ensured before starting new shiftMr Harwinder30/09/202430/09/2024Completed
OccuranceOpen Red Bin to be replaced with lock & key Red BinMr Harwinder30/09/202430/09/2024Completed
OccuranceWI to be displayed at Work StationMr Princ01/10/202401/10/2024Completed
OutflowQuality Alert to be displayed at "Q" GateMr Princ25/09/202425/09/2024Completed
OccuranceQuality Alert to be displayed at CNC SectionMr Princ25/09/202425/09/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% inspection of Groove Dia
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Open red bin was used.
1113_Occurance_Before.jpg
Occurance (After) Open Red Bin to be replaced with lock & key Red Bin.
1113_Occurance_After.jpg
Outflow (Before) Sampling inspection was followed for Groove dia.
1113_Outflow_Before.png
Outflow (After) 100% inspection of Groove dia is started at final inspection.
1113_Outflow_After.png
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All CNC Machine / Similar Model
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP, InspCheckSheet
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 5
Reason for submission HEAD SIDE SEAT PIPE BROKEN