QFR No - 8000892985
Defect Details
NC No. | 8000892985 |
NC Date | 25/09/2024 |
NC Submission Date | |
Part No. | F1LG00902B |
Part Name | SEAT PIPE -K86A |
Supplier Name & Code | 100538-NARINDER PARKASH AND CO |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | BROKEN-HEAD SIDE SEAT PIPE BROKEN |
1. Problem Description
Defect Description | Crack from head side |
Detection Stage | Receipt |
Problem Severity | Safety |
NG Quantity | 1 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@npcindustries.in |
Plant Head/CEO Email ID | anand@npcindustries.in |
MD Email ID | ajay@npcindustries.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
10000
|
15000
|
20000
|
15000
|
10000
|
70000
|
Check Qty |
10000
|
15000
|
20000
|
15000
|
10000
|
70000
|
NG Qty |
1
|
0
|
0
|
0
|
0
|
1
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% inspection of available material. |
3. Process Flow
Process Flow Description |
---|
1) Cutting 2) Draw 3) Head Formation 4) Punching 5) Rough Grinding 6) CNC Head Turning 7) CNC Boring & Facing 8) Tapping 9) Chamfering 10) Final Grinding 11) Final Inspection 12) Cleaning 13) Oiling 14) Packing & Dispatch |
4. Process Details
Process / Operation | CNC Head Turning |
Outsource | No |
Machine / Cell | CNC |
Machine / Cell No. | CNC Section |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Head formation pin depth more | It was observed that Head Formation Pin Depth is OK | O |
Method | Part with less wall thickness near groove skipped Final `Q` Gate during inspection | It was observed that part having less wall thickness near groove skipped Final `Q` Gate | X |
Machine | Stroke variation | No Stroke variation observed | O |
Material | Hardness more | Material Hardness observed 45HRB which is observed to be within range | O |
Method | Setting part got mixed | It was observed that setting part got mixed | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Head Broken part |
Why 2 | Crack on part |
Why 3 | Wall thickness got less |
Why 4 | Extra machining done |
Why 5 | Setting part |
Root Cause (Occurance) | Setting part |
Root Cause Analysis (Outflow)
Why 1 | Head Broken part |
Why 2 | Could not be detected at final inspection |
Why 3 | Skipped at Final `Q` Gate |
Why 4 | Skipped in Groove dia sampling inspection |
Why 5 | Groove dia sampling qty less |
Root Cause (Outflow) | Groove dia Sampling Qty less |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | 100% inspection of Groove dia to be done | Mr Toti | 02/10/2024 | 02/10/2024 | Completed |
Occurance | Proper disposal of setting parts to be ensured before starting new shift | Mr Harwinder | 30/09/2024 | 30/09/2024 | Completed |
Occurance | Open Red Bin to be replaced with lock & key Red Bin | Mr Harwinder | 30/09/2024 | 30/09/2024 | Completed |
Occurance | WI to be displayed at Work Station | Mr Princ | 01/10/2024 | 01/10/2024 | Completed |
Outflow | Quality Alert to be displayed at "Q" Gate | Mr Princ | 25/09/2024 | 25/09/2024 | Completed |
Occurance | Quality Alert to be displayed at CNC Section | Mr Princ | 25/09/2024 | 25/09/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% inspection of Groove Dia |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Open red bin was used. 1113_Occurance_Before.jpg |
Occurance (After) |
Open Red Bin to be replaced with lock & key Red Bin. 1113_Occurance_After.jpg |
Outflow (Before) |
Sampling inspection was followed for Groove dia. 1113_Outflow_Before.png |
Outflow (After) |
100% inspection of Groove dia is started at final inspection. 1113_Outflow_After.png |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All CNC Machine / Similar Model |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP, InspCheckSheet |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | 5 |
Reason for submission | HEAD SIDE SEAT PIPE BROKEN |