QFR No - 8000893359
Defect Details
NC No. | 8000893359 |
NC Date | 27/09/2024 |
NC Submission Date | |
Part No. | S2MX00812B |
Part Name | STEEL BUSH J1A & J1D |
Supplier Name & Code | 101255-MAHAVIR INDUSTRIES |
ETL Plant | 1118-ETL E-92,93 Suspension |
Defect Details | LENGTH UNDERSIZE-T.LENGTH U/S SPE=25.20-0.20 OBS=24.84 |
1. Problem Description
Defect Description | LENGTH UNDERSIZE-T.LENGTH U/S SPE=25.20-0.20 OBS=24.84 |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 79 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@mahavirind.co.in |
Plant Head/CEO Email ID | planthead@mahavirind.co.in |
MD Email ID |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
7000
|
0
|
0
|
0
|
0
|
7000
|
Check Qty |
7000
|
0
|
0
|
0
|
0
|
7000
|
NG Qty |
17
|
0
|
0
|
0
|
0
|
17
|
Scrap | 17 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All Suspected Material segregation at Customer End |
3. Process Flow
Process Flow Description |
---|
RM inward - store - Traub Parting -Chamfering - Plating-Final inspection - Packing - Dispatch - Transport |
4. Process Details
Process / Operation | Traub Parting |
Outsource | Yes |
Machine / Cell | Traub No. 5 |
Machine / Cell No. | Traub Section |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Unskilled operator | As per Skilled Matrix Operator is skilled | O |
Tool | Wrong Tool Insert Use | Correct carbide parting Tool Use But Tool Holding Issue | X |
Material | Wrong Grade And other grade Material Use | Correct Grade CEW-1 Material use . | O |
Method | Machining Process & Inspection Method Wrong | Machining Process is ok But Inspection Method Wrong | X |
Machine | Machine Condition Not OK | As per Daily Check sheet Machine Condition was OK | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Length oversize / under size |
Why 2 | During the parting process, the parting tool Insert is lightly loose on the Traub machine. |
Why 3 | The tool Insert is not properly tightened because the bolt head is worn due to improper tightening with an Allon Key |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | During the parting process, the parting tool Insert is lightly loose on the Traub machine. |
Root Cause Analysis (Outflow)
Why 1 | Length oversize / under size |
Why 2 | Sample Basis Inspection On final Inspection stage . |
Why 3 | No stage Wise Length gauges Only One Gauge For Both Stage |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | No stage Wise Length gauges Only One Gauge For Both Stage. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | New Parting Tool Holder Replace on Traub Machine and Insert change Work Instruction Display | Production Head | 30/09/2024 | 30/09/2024 | Completed |
Outflow | Additional New Length gauge Arrange On Final Inspection Stage for 100% Inspection. | Quality Head | 10/09/2024 | 06/09/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% Length Inspection on final Stage Instead of 50% Inspection |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
During the parting process, the parting tool Insert is lightly loose on the Traub machine. 1117_Occurance_Before.jpg |
Occurance (After) |
New Parting Tool Holder Replace on Traub Machine and Insert change Work Instruction Display 1117_Occurance_After.jpg |
Outflow (Before) |
No stage Wise Length gauges Only One Gauge For Both Stage . 1117_Outflow_Before.jpg |
Outflow (After) |
Additional New Length gauge Arrange On Final Inspection Stage for 100% Inspection. 1117_Outflow_After.docx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All Steel Bush |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | 200 |
Reason for submission | after taking action no any issue reported for the same. |