QFR No - 8000893366
Defect Details
NC No. 8000893366
NC Date 27/09/2024
NC Submission Date
Part No. S2DA00907O
Part Name TOP SPRING LOCATOR
Supplier Name & Code 100161-PREMIER ENGINEERS
ETL Plant 1118-ETL E-92,93 Suspension
Defect Details POWDER COATING NOT OK-POWDER COATING PEEL OFF
 
1. Problem Description
Defect Description POWDER COATING NOT OK-POWDER COATING PEEL OFF
Detection Stage Inprocess
Problem Severity Aesthetic
NG Quantity 1168
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality.premier@sanghavigroup.co.in
Plant Head/CEO Email ID prabhune.girish@sanghavigroup.co.in
MD Email ID sanghavi.rajesh@sanghavigroup.co.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1200
0
0
0
0
1200
Check Qty
1200
0
0
0
0
1200
NG Qty
1166
0
0
0
0
1166
 
Scrap 1166
Rework 0
Under Deviation 0
Containment Action
All the material available at Endurance End Segregated by hitting method
 
3. Process Flow
Process Flow Description
RM+Cutting+Forming+Piercing+Vibro+Powder Coating+Final Inspection
 
4. Process Details
Process / Operation Powder Coating at Krishna Coating
Outsource Yes
Machine / Cell Red wine locator Line
Machine / Cell No. Red wine locator
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodNo proper bonding of paint to LocatorAt phosphating stage bath concentration not maaintainedX
MethodOil traces on parts-tank heater not workingX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Inspection by nail
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5/100
7. Root Cause Analysis (Occurance)
Why 1 Coating Peel Off
Why 2 Phosphating observed week
Why 3 Bath concentration observed less
Why 4 regular bath analysis not done
Why 5 Lab chemist not done analysis
Root Cause (Occurance) Phosphating bath concentration not maintained.
 
Root Cause Analysis (Outflow)
Why 1 Coating Peel Off
Why 2 Part missed from inspector
Why 3 Part peel off not observed during Inspection
Why 4 Sampling basis adhesion verification
Why 5 sampling frequency not increased
Root Cause (Outflow) Due to sampling basis adhesion inspection part could not be cached at final inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccurancePhosphating bath concentration maintained, Degreasing heater StartedMr.Lokahnde01/10/202415/10/2024Completed
OutflowSampling frequency for Adhesion increased, Double sampling startedMr.Lokhande01/10/202415/10/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Double sampling inspection for adhesion started
Inspection Method Other
Other Inspection Method Cross Adhesion
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5/100
10. Evidance of Countermeasure
Occurance (Before) Phosphating Stage Bath Concentration not maintained and Degreasing Heater not working which is started.
1116_Occurance_Before.pdf
Occurance (After) Bath Concentration maintained and Heater Started
1116_Occurance_After.pdf
Outflow (Before) Operator Skill matrix Not Updated
1116_Outflow_Before.pdf
Outflow (After) Training Provided to Final Inspector
1116_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Brass Gold Locator, Silver Locator
 
12. Document Review
Documents WISOP
Specify Other Document OPL Implemented
 
13. Effectiveness Of Action
Reviewed Quantity 500
Reason for submission AFTER TAKING ACTION POWDER COATING FOUND OK- NO POWDER COATING PEEL OFF OBSERVED.