QFR No - 8000894558
Defect Details
NC No. 8000894558
NC Date 05/10/2024
NC Submission Date
Part No. F2FA28133M
Part Name FORK PIPE MACHINED - Ø37.1
Supplier Name & Code 100576-SANGKAJ BRIGHT WIRES PVT LTD
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-THREADING NG
 
1. Problem Description
Defect Description THREADING NG
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 22
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID brightwire.qa@sangkaj.com
Plant Head/CEO Email ID steel@sangkaj.com
MD Email ID anirudh.2007@hotmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
750
0
0
450
350
1550
Check Qty
750
0
0
450
350
1550
NG Qty
22
0
0
0
0
22
 
Scrap 22
Rework 0
Under Deviation 0
Containment Action
1) At ETL end verified the 750 nos out of 22 nos found defective.2) At SBWPL end verified the 800 nos all part found ok. 3) for ok part provided the identification mark.
 
3. Process Flow
Process Flow Description
Receipt Of Material - Inward Inspection - CNC 1st Setup - CNC 2nd Setup - Drilling - Final Inspection - Air Cleaning - Dispatch
 
4. Process Details
Process / Operation CNC 2nd Setup
Outsource No
Machine / Cell Machining
Machine / Cell No. Fork Pipe Machining
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManDue to Inspector negligence.Verified found not okX
ToolTool holder looseVerified OkO
ToolInsert Wear OutVerified OkO
MethodPart Touch with stand, No arrangement to avoid the fork pipe contact with standVerified found not okX
MachineSpindle run out not okVerified OkO
ManNew OperatorVerified OkO
MaterialMaterial grade not okVerified OkO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Fork Pipe threading NG
Why 2 Thread ring gauge not qualify
Why 3 Dent on threading
Why 4 Fork pipe directly kept on Metal stand
Why 5 No arrangement to avoid the contact of stand & fork pipe.
Root Cause (Occurance) No arrangement to avoid the contact of stand & fork pipe.
 
Root Cause Analysis (Outflow)
Why 1 Fork Pipe threading NG
Why 2 Skipped from inspector.
Why 3 Due to Inspector negligence.
Why 4
Why 5
Root Cause (Outflow) Due to Inspector negligence.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Outflow1) Identification mark provided after final inspection for threading ok 2) Display OPL at machining & final Inspection stage.Mr. Nitin Puri11/10/202411/10/2024Completed
OccuranceBlue sheet provided to avoid the threading damage issue.Mr. Barik & Mr. Nitin Puri11/10/202411/10/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details No Change
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size PDIR
10. Evidance of Countermeasure
Occurance (Before) Fork pipe kept on stand,No arrangement for avoid the threading damage
1138_Occurance_Before.xlsx
Occurance (After) Blue sheet provided to avoid the threading damage issue.
1138_Occurance_After.xlsx
Outflow (Before) Identification mark not provided after final inspection.
1138_Outflow_Before.xlsx
Outflow (After) 1) Identification mark provided after final inspection for threading ok 2) Display OPL at machining & final Inspection stage.
1138_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All model
 
12. Document Review
Documents WISOP
Specify Other Document Display OPL
 
13. Effectiveness Of Action
Reviewed Quantity 120
Reason for submission Verified next lot observed ok