QFR No - 8000894559
Defect Details
NC No. | 8000894559 |
NC Date | 05/10/2024 |
NC Submission Date | |
Part No. | 550FA12233 |
Part Name | FORK PIPE MACHINED - K3 |
Supplier Name & Code | 100576-SANGKAJ BRIGHT WIRES PVT LTD |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-SHORT LENGTH |
1. Problem Description
Defect Description | SHORT LENGTH |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 27 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | brightwire.qa@sangakj.com |
Plant Head/CEO Email ID | steel@sangkaj.com |
MD Email ID | anirudh.2007@hotmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
750
|
0
|
0
|
1200
|
650
|
2600
|
Check Qty |
750
|
0
|
0
|
0
|
0
|
750
|
NG Qty |
27
|
0
|
0
|
0
|
0
|
27
|
Scrap | 27 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
1) At ETL end verified 750 nos out of 27 nos found defective 2) At SBWPL end verified 1850 nos foun ok. 3) Provided identification mark on ok part. |
3. Process Flow
Process Flow Description |
---|
Receipt of Material - inward inspection - CNC 1st Setup - CNC 2nd Setup - Ø5 Drilling - Final Inspection - Air Cleaning - Dispatch |
4. Process Details
Process / Operation | CNC 2nd Setup |
Outsource | No |
Machine / Cell | CNC Cell |
Machine / Cell No. | Fork Pipe Cell |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | New Operator | Verified Ok | O |
Machine | Wrong offset | Verified ok | O |
Material | Wrong material Received | Verified Ok | O |
Man | Inspector/ operator negligence-during Inspection/ process | Verified found not ok | X |
Method | No arrangement to remove the stopper stick burr | Verified found not ok | X |
Tool | Insert Wear Out | Verified found ok | O |
6. Inspection Method Analysis (Current)
Inspection Method | Sp. Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Fork pipe short length |
Why 2 | Fork pipe not properly rest on stopper face |
Why 3 | Machining loose burr stack on stopper face |
Why 4 | No arrangement to remove the stopper stack burr. |
Why 5 | |
Root Cause (Occurance) | No arrangement to remove the stopper stack burr. |
Root Cause Analysis (Outflow)
Why 1 | Fork pipe short length |
Why 2 | Skipped from operator & inspector. |
Why 3 | Due to operator & inspector negligence. |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Due to operator & inspector negligence. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Air flushing provided on CNC machining to remove the stack burr. | Mr. Barik & Mr. Nitin Puri | 11/10/2024 | 11/10/2024 | Completed |
Outflow | 1) 100% inspection with the help of Spl gauge at machining stage 100% & final inspection doing 15 days. | Mr. Nitin Puri | 11/10/2024 | 11/10/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | No Change in inspection method |
Inspection Method | Sp. Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
No arrangement of air flushing to remove the stuck burr. 1135_Occurance_Before.xlsx |
Occurance (After) |
Provided Air flushining rrangement to remove the stuck burr. 1135_Occurance_After.xlsx |
Outflow (Before) |
Identification mark not provided after final inspection. 1135_Outflow_Before.xlsx |
Outflow (After) |
1) Identification mark provided after final inspection.
2) 100% inspection with the help of spl. height gauge.
3) Sampling Basis inspection with the help of DHG 1135_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Applicable all model & machine |
12. Document Review
Documents | WISOP |
Specify Other Document | Display OPL |
13. Effectiveness Of Action
Reviewed Quantity | 58 |
Reason for submission | Verified lot found Ok |