QFR No - 8000895936
Defect Details
NC No. 8000895936
NC Date 17/10/2024
NC Submission Date
Part No. 550PJ00102
Part Name VALVE SEAT
Supplier Name & Code 100990-JAIRAJ ANCILLARIES PVT LTD
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-HOLE
 
1. Problem Description
Defect Description Hole observed in part surface
Detection Stage Inprocess
Problem Severity Function
NG Quantity 42
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID planthead.aurangabad@jairajgroup.com
Plant Head/CEO Email ID vp@jairajgroup.com
MD Email ID rajiv@jairajgroup.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
5000
0
0
1000
0
6000
Check Qty
5000
0
0
1000
0
6000
NG Qty
42
0
0
5
0
47
 
Scrap 47
Rework 0
Under Deviation 0
Containment Action
All available stock at ETL checked 100% and found 47 no. defective parts out of 5000 no. checked. Also checked 100% FG stock inhouse & found 5 parts defective.
 
3. Process Flow
Process Flow Description
Injection Moulding
 
4. Process Details
Process / Operation Injection Moulding
Outsource No
Machine / Cell Injection Moulding
Machine / Cell No. IMM-01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineClamping pressure lowVerified as per CP & OCS found ok, as per standard specificationO
MachineOCS & Control plan not followed by machine operatorVerified as per CP & OCS found ok, as per standard specificationO
MethodSampling InspectionVerified & found that defects are checked on sampling basisX
ManMan power does not aware about this defectVerified that operator, In process inspector & final inspector are aware of this defectO
ToolCore cavity butting not adequateChecked with blue matching and found okO
ToolEjector pin butting in cavity after mould clampingVerified and found ejector pin head bend and butt in cavityX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Sampling
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5
7. Root Cause Analysis (Occurance)
Why 1 Hole on part due to Ejector pin butt in cavity
Why 2 Due to Ejector pin head broken
Why 3 Due to Ejector pin came out from Ejector assembly
Why 4 Due to Round shape Head the Head loose due to continuous to & fro motion.
Why 5 Round shape head loose & came out from locking plate.
Root Cause (Occurance) Due to Round shape Head , it came out from locking plate & loosened resulting in butting with cavity..
 
Root Cause Analysis (Outflow)
Why 1 Hole on part not captured during final Inspection.
Why 2 Part checked on Sampling basis
Why 3 Checking method inadequate for hole defect.
Why 4
Why 5
Root Cause (Outflow) Checking method inadequate for hole defect.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceEjector Pin Head changed from Round shape to D shapeGanesh Mhaske18/10/202418/10/2024Completed
OccuranceGiven training to operator to check the part in process for Hole by visual inspection and given instruction for not to run the production if he found any out of tolerance .Mr Sandip Rode18/10/202418/10/2024Completed
OutflowInspection standard displayed on machine as well as firewall inspection stationsSandip Rode19/10/202419/10/2024Completed
OutflowGiven on job training to Inspector to check the parts 100% for visual inspection for hole and aesthetic defects and Given instruction not to pass .Sandip Rode19/10/202419/10/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% Inspection at firewall through Visual Inspection.
Inspection Method Other
Other Inspection Method 100% Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Before -Earlier Ejector Pin head as Round shape resulting in loosening from locking plate with to & from motion .
1154_Occurance_Before.jpg
Occurance (After) After - Ejector Pin Head changed from Round Shape to D Shape.
1154_Occurance_After.jpg
Outflow (Before) Inspection is on Sampling basis.
1154_Outflow_Before.pdf
Outflow (After) Inspection is 100 % and Inspection standard, PFMEA , CP updated
1154_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NIL
 
12. Document Review
Documents ControlPlan, PFMEA, InspCheckSheet
Specify Other Document NIL
 
13. Effectiveness Of Action
Reviewed Quantity 50
Reason for submission 5. Problem Analysis - Judgment not ok - Provide `O` for OK judgment and `X` for NG 7. Root Cause Analysis (Occurrence) - Due to Round shape Head the Head loose - Why loose? 8. Countermeasure ( Occurrence , Outflow & System side Actions ) Ejector Pin Head changed from Round shape to D shape - Validation missing?