QFR No - 8000895946
Defect Details
NC No. | 8000895946 |
NC Date | 17/10/2024 |
NC Submission Date | |
Part No. | 520BZ01102 |
Part Name | CAP OIL LOCK (K3) |
Supplier Name & Code | 100161-PREMIER ENGINEERS |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-MIXUP |
1. Problem Description
Defect Description | Specification - No identification groove required Observed – Identification groove observed |
Detection Stage | Inprocess |
Problem Severity | Aesthetic |
NG Quantity | 3 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | Quality.premier@sanghavigroup.co.in |
Plant Head/CEO Email ID | prabhune.girish@sanghavigroup.co.in |
MD Email ID | sanghavi.rajesh@sanghavigroup.co.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1000
|
0
|
0
|
0
|
0
|
1000
|
Check Qty |
1000
|
0
|
0
|
0
|
0
|
1000
|
NG Qty |
3
|
0
|
0
|
0
|
0
|
3
|
Scrap | 3 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Available lot Segregated at customer end for Identification marking On OD. |
3. Process Flow
Process Flow Description |
---|
Raw Tube+Angle forming + close end forming+Grinding |
4. Process Details
Process / Operation | Grinding |
Outsource | No |
Machine / Cell | Grinding Machine 01 |
Machine / Cell No. | 01 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Identification provided on part on sampling basis | Identification ring provided on part | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 |
7. Root Cause Analysis (Occurance)
Why 1 | Ring mark On cap Oil Lock OD |
Why 2 | For part identification, sampling basis ring provided on part. |
Why 3 | sample part mixed with regular part |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Identification groove ID part mixed with regular part |
Root Cause Analysis (Outflow)
Why 1 | Ring mark on oD |
Why 2 | Inspector not identified Groove on part |
Why 3 | Sampling basis Inspection |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Sampling basis Inspection |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Trial part will be kept separately | Mr.Balraj | 28/10/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Separate Identification |
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 |
10. Evidance of Countermeasure
Occurance (Before) |
No Ring mark Verification 1158_Occurance_Before.pdf |
Occurance (After) |
Ring mark verification at Set up started 1158_Occurance_After.pdf |
Outflow (Before) |
No Inspector Training 1158_Outflow_Before.pdf |
Outflow (After) |
Final Inspector Training provided 1158_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Grinding machine |
12. Document Review
Documents | WISOP |
Specify Other Document | One point lesson |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | 5. Problem Analysis - Need all 4M |