QFR No - 8000895946
Defect Details
NC No. 8000895946
NC Date 17/10/2024
NC Submission Date
Part No. 520BZ01102
Part Name CAP OIL LOCK (K3)
Supplier Name & Code 100161-PREMIER ENGINEERS
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-MIXUP
 
1. Problem Description
Defect Description Specification - No identification groove required Observed – Identification groove observed
Detection Stage Inprocess
Problem Severity Aesthetic
NG Quantity 3
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID Quality.premier@sanghavigroup.co.in
Plant Head/CEO Email ID prabhune.girish@sanghavigroup.co.in
MD Email ID sanghavi.rajesh@sanghavigroup.co.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
0
0
0
0
1000
Check Qty
1000
0
0
0
0
1000
NG Qty
3
0
0
0
0
3
 
Scrap 3
Rework 0
Under Deviation 0
Containment Action
Available lot Segregated at customer end for Identification marking On OD.
 
3. Process Flow
Process Flow Description
Raw Tube+Angle forming + close end forming+Grinding
 
4. Process Details
Process / Operation Grinding
Outsource No
Machine / Cell Grinding Machine 01
Machine / Cell No. 01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineIdentification provided on part on sampling basisIdentification ring provided on partO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100
7. Root Cause Analysis (Occurance)
Why 1 Ring mark On cap Oil Lock OD
Why 2 For part identification, sampling basis ring provided on part.
Why 3 sample part mixed with regular part
Why 4
Why 5
Root Cause (Occurance) Identification groove ID part mixed with regular part
 
Root Cause Analysis (Outflow)
Why 1 Ring mark on oD
Why 2 Inspector not identified Groove on part
Why 3 Sampling basis Inspection
Why 4
Why 5
Root Cause (Outflow) Sampling basis Inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceTrial part will be kept separatelyMr.Balraj28/10/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Separate Identification
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100
10. Evidance of Countermeasure
Occurance (Before) No Ring mark Verification
1158_Occurance_Before.pdf
Occurance (After) Ring mark verification at Set up started
1158_Occurance_After.pdf
Outflow (Before) No Inspector Training
1158_Outflow_Before.pdf
Outflow (After) Final Inspector Training provided
1158_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Grinding machine
 
12. Document Review
Documents WISOP
Specify Other Document One point lesson
 
13. Effectiveness Of Action
Reviewed Quantity 50
Reason for submission 5. Problem Analysis - Need all 4M