QFR No - 8000896101
Defect Details
NC No. 8000896101
NC Date 17/10/2024
NC Submission Date
Part No. F2PH01202B
Part Name valve retainer for K10 Ø18
Supplier Name & Code 100161-PREMIER ENGINEERS
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-OD OVERSIZE
 
1. Problem Description
Defect Description OD oversize Specification - 38.85 ±0.05 Observed - 39.074
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 5
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality.premier@sanghavigroup.co.in
Plant Head/CEO Email ID prabhune.girish@sanghavigroup.co.in
MD Email ID sanghavi.rajesh@sanghavigroup.co.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1500
0
0
0
0
1500
Check Qty
1500
0
0
0
0
1500
NG Qty
5
0
0
0
0
5
 
Scrap 5
Rework 0
Under Deviation 0
Containment Action
Available parts at Endurance send Segregated with Meting part.
 
3. Process Flow
Process Flow Description
Raw material+CNC+Forming and Piercing+CNC
 
4. Process Details
Process / Operation CNC
Outsource No
Machine / Cell CNC 03
Machine / Cell No. CNC Machine
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodImproper part ClampingDuring CNC part observed improper clamping during CNC operationX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Digital VC
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 20/100
7. Root Cause Analysis (Occurance)
Why 1 OD oversize
Why 2 Due to part OD ovality
Why 3 Due Part loading during CNC
Why 4 part improper clamping
Why 5 Operator not aware about Part ovality
Root Cause (Occurance) Improper clamping of part during CNC operation.
 
Root Cause Analysis (Outflow)
Why 1 OD oversize
Why 2 part verification on sampling basis
Why 3 No Inspector awareness for OD oversize
Why 4 Awareness training provided to Inspector
Why 5
Root Cause (Outflow) Sampling basis OD Inspection.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceOn CNC part clamping training provided to OperatorMr.Vilas Kamble25/10/2024Completed
OutflowSampling quantity increased Double sampling followed.Mrs.Deshmukh25/10/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Double sampling followed
Inspection Method Other
Other Inspection Method 20/100 part Insp
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 20/100
10. Evidance of Countermeasure
Occurance (Before) After Set up no verification
1166_Occurance_Before.pdf
Occurance (After) After Set Up verification Started.
1166_Occurance_After.pdf
Outflow (Before) Sampling Basis Inspection
1166_Outflow_Before.pdf
Outflow (After) Sampling frequency Increased
1166_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant CNC MAchine 02
 
12. Document Review
Documents WISOP
Specify Other Document One Point Lesson
 
13. Effectiveness Of Action
Reviewed Quantity 50
Reason for submission 5. Problem Analysis - Need to cover all 4M