QFR No - 8000896112
Defect Details
NC No. | 8000896112 |
NC Date | 17/10/2024 |
NC Submission Date | |
Part No. | F2KH01002B |
Part Name | REBOUND SPRING-XF121 |
Supplier Name & Code | 101159-TECHNOMAT SPRINGS |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | BEND-BEND |
1. Problem Description
Defect Description | Bend |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 6 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | quality@technomatsprings.com |
Plant Head/CEO Email ID | technomatsprings@gmail.com |
MD Email ID | patilsadanand@technomatsprings.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
15000
|
0
|
0
|
28000
|
0
|
43000
|
Check Qty |
15000
|
0
|
0
|
28000
|
0
|
43000
|
NG Qty |
6
|
0
|
0
|
0
|
0
|
6
|
Scrap | 6 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Checked all material at customer end and pipeline material also. |
3. Process Flow
Process Flow Description |
---|
R/m In-warding Inspection > Coiling > Stress Relieving-1 > Grinding > Shot Peening > Stress Relieving-2 > Final Inspection > Oiling > Packing > Dispatch. |
4. Process Details
Process / Operation | coiling |
Outsource | No |
Machine / Cell | - |
Machine / Cell No. | - |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Material | Wrong Material / Grade | Supplier RMTC Report checked found Ok | O |
Man | Unskilled Operator | Skilled matrix found ok | O |
Tool | Tool Loose / Tool thread wear out | found pitch tool locking bolt thread wear out | X |
Machine | Machine check Sheet not followed | Found machine JH activity done as per the mentioned freq. | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 50 Nos |
7. Root Cause Analysis (Occurance)
Why 1 | Un-Grounded Spring observed. |
Why 2 | Grinding operation not done. |
Why 3 | spring length undersized in coiling operation. |
Why 4 | Due to pitch tool locking thread wear out. |
Why 5 | No check point available for thread locking wear out in JH check sheet. |
Root Cause (Occurance) | No check point available for thread locking wear out in JH check sheet. |
Root Cause Analysis (Outflow)
Why 1 | Un-Grounded Spring observed. |
Why 2 | Defective parts escaped from inspection. |
Why 3 | Defective parts was few due to that not arrested in insp. |
Why 4 | Inspection Done on sampling Basis. |
Why 5 | |
Root Cause (Outflow) | Inspection done on sampling basis and defective parts were less so not arrested in final inspection. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | 100% Visual Inspection started. | Mr. Anuj Shelke | 07/11/2024 | 07/11/2024 | Inprocess |
Occurance | Check point added in JH check sheet. | Mr. Khandare | 07/11/2024 | 07/11/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% visual inspection started. |
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
In the JH check sheet,the nut bolt looseness point was not mentioned. 1167_Occurance_Before.xlsb |
Occurance (After) |
In the JH check sheet, nut bolt looseness point has been added. 1167_Occurance_After.xlsb |
Outflow (Before) |
Inspection done as per the sampling plan. 1167_Outflow_Before.xlsb |
Outflow (After) |
100% inspection has started. 1167_Outflow_After.xlsb |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Horizontally deployed for the all similar machines. |
12. Document Review
Documents | JHCheckSheet |
Specify Other Document | NA |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |