QFR No - 8000896118
Defect Details
NC No. | 8000896118 |
NC Date | 17/10/2024 |
NC Submission Date | |
Part No. | F2FQ00507B |
Part Name | HOLDER HANDLE P/C-XF-1C1 |
Supplier Name & Code | 100001-ANANT ENTERPRISES |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | B/H INSIDE BORE-BLOW HOLE,CUT MARK |
1. Problem Description
Defect Description | CUT MARK |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 70 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | anandkulkarni@anantgroup.co.in |
Plant Head/CEO Email ID | pramodgosavi@anantgroup.co.in |
MD Email ID | ashwinjoshi@anantgroup.co.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
0
|
0
|
0
|
205
|
160
|
365
|
Check Qty |
0
|
0
|
0
|
203
|
152
|
355
|
NG Qty |
0
|
0
|
0
|
2
|
8
|
10
|
Scrap | 10 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
Under cut part segregated at our end and scraped separately for the same. ICA mark started back side on part surface for the confirm free from cut mark on part. |
3. Process Flow
Process Flow Description |
---|
Raw material Inspection=Melting=Spectro=Metal transfer to holding furnace=Degassing=Die preparation=Casting=Riser cutting=Inspection=Buffing=Heat treatment=Inspection=Powder coating=Inspection=Machining=deburring=Pre-Washing=Final Inspection=Packing Dispatched |
4. Process Details
Process / Operation | Casting=HT=PC=M/C |
Outsource | No |
Machine / Cell | Plat Form number 03 |
Machine / Cell No. | Machine Number 04 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Unskilled manpower | Skill matrix verified and found ok | O |
Method | Buffing process | Buffing process done by manual, some part profile not matched during buffing | X |
Material | Material not ok | Material grade check and found as per specification. | O |
Machine | Machine condition not ok | Machine condition verified and PM done as per defined frequency | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | cut mark observed on part |
Why 2 | Cut mark observed on part due to buffing not done properly |
Why 3 | Buffing not done properly due to buffing process is manual |
Why 4 | Buffing process is manual due to some part profile not match process |
Why 5 | |
Root Cause (Occurance) | Buffing process is manual due to some part profile not match in process |
Root Cause Analysis (Outflow)
Why 1 | Cut mark observed on part |
Why 2 | Cut mark part skipped by inspector |
Why 3 | Part skipped by inspector due to part not catch by inspector at final stage |
Why 4 | cut mark part not catch by inspector due to eyes sequence not followed |
Why 5 | Eyes sequence not followed due to operator negligence |
Root Cause (Outflow) | Eyes sequence not followed due to operator negligence |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | Q- alert displayed | Nisar | 19/10/2024 | 19/10/2024 | Completed |
Outflow | Awareness training given to all Inspector regarding customer complaint. | Nisar A | 20/10/2024 | 20/10/2024 | Completed |
Occurance | Q alert and defect matrix displayed | Nisar A. | 19/10/2024 | 19/10/2024 | Completed |
Occurance | Start to five numbers part check in every hrs in buffing process. | Ambar | 22/10/2024 | 22/10/2024 | Completed |
Occurance | Training has given to all buffing operator regarding customer complaint | Nisar A. | 20/10/2024 | 20/10/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | No any change in process |
Inspection Method | Other |
Other Inspection Method | Visual inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Q- alert display 1173_Occurance_Before.pdf |
Occurance (After) |
Training given to al regarding customer complaint 1173_Occurance_After.pdf |
Outflow (Before) |
Q alert displayed 1173_Outflow_Before.pdf |
Outflow (After) |
Awareness training given to al inspector regarding customer complaint 1173_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All holder and bracket |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP |
Specify Other Document | No Any |
13. Effectiveness Of Action
Reviewed Quantity | 50 |
Reason for submission | ok |