QFR No - 8000902820
Defect Details
NC No. | 8000902820 |
NC Date | 09/12/2024 |
NC Submission Date | |
Part No. | F2DZ03112B |
Part Name | FORK BOLT |
Supplier Name & Code | 101263-SINGLA PRECISION SCREWS |
ETL Plant | 1117-ETL K-228/9 Suspension |
Defect Details | NOT AS PER SPECIFICATION-THREADING CONCENTRICITY MORE |
1. Problem Description
Defect Description | THRADING CONCENTRICITY MORE |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 106 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo | 3tkupsqk0tnofazl2odnzfet.jpg |
Supplier Communication Details
Quality Head Email ID | quality@singlaprecision.com |
Plant Head/CEO Email ID | quality@singlaprecision.com |
MD Email ID | aditya@singlaprecision.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
2000
|
5000
|
0
|
5000
|
3000
|
15000
|
Check Qty |
2000
|
5000
|
0
|
5000
|
3000
|
15000
|
NG Qty |
106
|
0
|
0
|
0
|
0
|
106
|
Scrap | 106 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
WE ARE ALL MATERIAL SEGGRATION CUSTOMER AND OUR END |
3. Process Flow
Process Flow Description |
---|
RAW MATERIAL+CUTTING+FORGING+CNC 1ST+CNC 2ND+ROLLING+ SURFACE TREATMENT +FINAL INSPECTION+ PACKING |
4. Process Details
Process / Operation | ROLLING |
Outsource | No |
Machine / Cell | ROLLING |
Machine / Cell No. | 01 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | MACHINE ROLLING TOOL NOT ALIGMENT PROPERLY | VALIDATION AND FOUND OK | O |
Material | MACHINE OUTPUT MATERAIL HANDLING NOT PROPERLY | VALIDATION AND FOUND OK | O |
Man | UNAWARENESS OF OPERATOR | VALIDATION AND FOUND OPERATOR SKILL LEVEL OK | O |
Tool | ROLLING MACHINE PART STOPER TOOL WEAR OUT | VALIDATION AND FOUND NG | X |
Method | MACHINE ROLLING PROCESS THREAD NOT CHECKED 100% | VALIDATION AND FOUND NG | X |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | NOT AS PER SPECIFICATION-THREADING CONCENTRICITY MORE |
Why 2 | ROLLING MACHINE SETTING TIME PART STOPER NOT CHECKING |
Why 3 | ROLLING MACHINE PART STOPER WEAR OUT |
Why 4 | SO PART ARE NOT INSERT AS PER ROLLING DIE STOPER PROPERLY |
Why 5 | ROLLING MACHINE ARE NOT STOPER CARBITE MATERIAL |
Root Cause (Occurance) | ROLLING MACHINE PART STOPER WEAR OUT |
Root Cause Analysis (Outflow)
Why 1 | NOT AS PER SPECIFICATION-THREADING CONCENTRICITY MORE |
Why 2 | ROLLING MACHINE SETTING TIME ROLLING DIE AND PART STOPER ALIGMENT NOT CHECKING POINT AVAILABLE AS PER QC CHECK SHEET |
Why 3 | MACHINE ROLLING PROCESS THREAD NOT CHECKED 100% |
Why 4 | ROLLING MACHINE PART AFTER THREAD AS PER CUSTMONER SPECIFACTION THREAD GAUGE NOT AVALILABLE |
Why 5 | MASTER GAUGE ARE NOT MADE AS PER ASEMBLE PROCESS |
Root Cause (Outflow) | ROLLING MACHINE PART AFTER THREAD AS PER CUSTMONER SPECIFACTION THREAD GAUGE NOT AVALILABLE |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | ROLLING MACHINE ALL FORK BOLT PART STOPER PROVIDE CARBITE MATERIAL | MR. ANIL | 14/12/2024 | 14/12/2024 | Completed |
Outflow | AS PER CUSTMONER SPECIFACTION THREAD GAUGE PROVIDE ON MACHINE | MR.GANESH MAURYA | 14/12/2024 | 14/12/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% TRG CHECK IN FINAL INSPECTION |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
ROLLING MACHINE ALL FORK BOLT PART STOPER NOT PROVIDE CARBITE MATERIAL 1267_Occurance_Before.xlsx |
Occurance (After) |
ROLLING MACHINE ALL FORK BOLT PART STOPER PROVIDE CARBITE MATERIAL 1267_Occurance_After.xlsx |
Outflow (Before) |
AS PER CUSTMONER SPECIFACTION THREAD GAUGE NOT AVAILABLE ON MACHINE 1267_Outflow_Before.xlsx |
Outflow (After) |
AS PER CUSTMONER SPECIFACTION THREAD GAUGE PROVIDE ON MACHINE 1267_Outflow_After.xlsx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | FORK BOLT ALL MODEL |
12. Document Review
Documents | ControlPlan, PFMEA, InspCheckSheet |
Specify Other Document | N/A |
13. Effectiveness Of Action
Reviewed Quantity | 100 |
Reason for submission | ok |