QFR No - 8000902820
Defect Details
NC No. 8000902820
NC Date 09/12/2024
NC Submission Date
Part No. F2DZ03112B
Part Name FORK BOLT
Supplier Name & Code 101263-SINGLA PRECISION SCREWS
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-THREADING CONCENTRICITY MORE
 
1. Problem Description
Defect Description THRADING CONCENTRICITY MORE
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 106
Is Defect Repeatative? Yes
Defect Sketch / Photo 3tkupsqk0tnofazl2odnzfet.jpg
Supplier Communication Details
Quality Head Email ID quality@singlaprecision.com
Plant Head/CEO Email ID quality@singlaprecision.com
MD Email ID aditya@singlaprecision.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
2000
5000
0
5000
3000
15000
Check Qty
2000
5000
0
5000
3000
15000
NG Qty
106
0
0
0
0
106
 
Scrap 106
Rework 0
Under Deviation 0
Containment Action
WE ARE ALL MATERIAL SEGGRATION CUSTOMER AND OUR END
 
3. Process Flow
Process Flow Description
RAW MATERIAL+CUTTING+FORGING+CNC 1ST+CNC 2ND+ROLLING+ SURFACE TREATMENT +FINAL INSPECTION+ PACKING
 
4. Process Details
Process / Operation ROLLING
Outsource No
Machine / Cell ROLLING
Machine / Cell No. 01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineMACHINE ROLLING TOOL NOT ALIGMENT PROPERLYVALIDATION AND FOUND OKO
MaterialMACHINE OUTPUT MATERAIL HANDLING NOT PROPERLYVALIDATION AND FOUND OKO
ManUNAWARENESS OF OPERATORVALIDATION AND FOUND OPERATOR SKILL LEVEL OKO
ToolROLLING MACHINE PART STOPER TOOL WEAR OUTVALIDATION AND FOUND NGX
MethodMACHINE ROLLING PROCESS THREAD NOT CHECKED 100%VALIDATION AND FOUND NGX
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 NOT AS PER SPECIFICATION-THREADING CONCENTRICITY MORE
Why 2 ROLLING MACHINE SETTING TIME PART STOPER NOT CHECKING
Why 3 ROLLING MACHINE PART STOPER WEAR OUT
Why 4 SO PART ARE NOT INSERT AS PER ROLLING DIE STOPER PROPERLY
Why 5 ROLLING MACHINE ARE NOT STOPER CARBITE MATERIAL
Root Cause (Occurance) ROLLING MACHINE PART STOPER WEAR OUT
 
Root Cause Analysis (Outflow)
Why 1 NOT AS PER SPECIFICATION-THREADING CONCENTRICITY MORE
Why 2 ROLLING MACHINE SETTING TIME ROLLING DIE AND PART STOPER ALIGMENT NOT CHECKING POINT AVAILABLE AS PER QC CHECK SHEET
Why 3 MACHINE ROLLING PROCESS THREAD NOT CHECKED 100%
Why 4 ROLLING MACHINE PART AFTER THREAD AS PER CUSTMONER SPECIFACTION THREAD GAUGE NOT AVALILABLE
Why 5 MASTER GAUGE ARE NOT MADE AS PER ASEMBLE PROCESS
Root Cause (Outflow) ROLLING MACHINE PART AFTER THREAD AS PER CUSTMONER SPECIFACTION THREAD GAUGE NOT AVALILABLE
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceROLLING MACHINE ALL FORK BOLT PART STOPER PROVIDE CARBITE MATERIALMR. ANIL14/12/202414/12/2024Completed
OutflowAS PER CUSTMONER SPECIFACTION THREAD GAUGE PROVIDE ON MACHINEMR.GANESH MAURYA14/12/202414/12/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% TRG CHECK IN FINAL INSPECTION
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) ROLLING MACHINE ALL FORK BOLT PART STOPER NOT PROVIDE CARBITE MATERIAL
1267_Occurance_Before.xlsx
Occurance (After) ROLLING MACHINE ALL FORK BOLT PART STOPER PROVIDE CARBITE MATERIAL
1267_Occurance_After.xlsx
Outflow (Before) AS PER CUSTMONER SPECIFACTION THREAD GAUGE NOT AVAILABLE ON MACHINE
1267_Outflow_Before.xlsx
Outflow (After) AS PER CUSTMONER SPECIFACTION THREAD GAUGE PROVIDE ON MACHINE
1267_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant FORK BOLT ALL MODEL
 
12. Document Review
Documents ControlPlan, PFMEA, InspCheckSheet
Specify Other Document N/A
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission ok