QFR No - 7000839800
Defect Details
NC No. | 7000839800 |
NC Date | 30/05/2022 |
NC Submission Date | |
Part No. | C2PP00320B |
Part Name | WHEEL CLUTCH_C20009_D1 |
Supplier Name & Code | 100432-BHAKTI AUTO COMP PRIVATE LIMIT |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | PCD SHIFT-PCD GAUGE NOT QUALIFY |
1. Problem Description
Defect Description | Part are not qualifying to PCD gauge |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 40 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | sales@bhaktiauto.com |
Plant Head/CEO Email ID | sales@bhaktiauto.com |
MD Email ID | vinodanin@gmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
300
|
0
|
0
|
500
|
0
|
800
|
Check Qty |
300
|
0
|
0
|
500
|
0
|
800
|
NG Qty |
1
|
0
|
0
|
1
|
0
|
2
|
Scrap | 2 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% Inspection at final inspection stage |
3. Process Flow
Process Flow Description |
---|
Pressure Die casting-fettling-machining-Drilling-Tapping-Inspection-dispatch |
4. Process Details
Process / Operation | Drilling/Tapping |
Outsource | Yes |
Machine / Cell | VMC |
Machine / Cell No. | VMC cell |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Part Orientation of fixture | Part orientation is at casting oil hole | O |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | PCD Not Ok |
Why 2 | Part not located properly on fixture |
Why 3 | part locating in on casting oil hole |
Why 4 | oil hole has more clearance |
Why 5 | Non precise parameter |
Root Cause (Occurance) | part not mounted properly in its position on fixture. |
Root Cause Analysis (Outflow)
Why 1 | PCD not ok |
Why 2 | part inspection missing |
Why 3 | final inspection not done |
Why 4 | sampling inspection |
Why 5 | |
Root Cause (Outflow) | Sampling inspection hence part not detected in final inspection |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | PCD inspection 100% to be done at final inspection | Bhakti Auto | 01/06/2022 | 01/06/2022 | Completed |
Occurance | Part orientation locator to be change | OM Mahabali | 15/06/2022 | 15/06/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | PCD gauge 100% inspection implemented instead of sampling |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Pin Locator 157_Occurance_Before.pdf |
Occurance (After) |
Spring mechanism locator 157_Occurance_After.pdf |
Outflow (Before) |
Sampling Inspection 157_Outflow_Before.pdf |
Outflow (After) |
100% Inspection 157_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | No |
12. Document Review
Documents | ControlPlan |
Specify Other Document | x |
13. Effectiveness Of Action
Reviewed Quantity | 2000 |
Reason for submission | OK |