QFR No - 7000873898
Defect Details
NC No. | 7000873898 |
NC Date | 02/11/2022 |
NC Submission Date | |
Part No. | 533BW00102 |
Part Name | BUMP STOP |
Supplier Name & Code | 101023-FORES ELASTOMECH INDIA PVT. LT |
ETL Plant | 1126-ETL Pantnagar |
Defect Details | DAMAGES-Flashes and cut marks |
1. Problem Description
Defect Description | Flash and cut mark |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 1140 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo | 1y2tfrc3sjh55rzkgshxu2me.jpg |
Supplier Communication Details
Quality Head Email ID | malani.pritam@foresgroup.com |
Plant Head/CEO Email ID | singh.barinder@foresgroup.com |
MD Email ID | swamy.pj@foresgroup.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
20000
|
0
|
0
|
8000
|
0
|
28000
|
Check Qty |
1140
|
0
|
0
|
8000
|
0
|
9140
|
NG Qty |
1140
|
0
|
0
|
44
|
0
|
1184
|
Scrap | 1184 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100 % sorting done at M/s ETL End with third party & also sorting done at Fores End. |
3. Process Flow
Process Flow Description |
---|
Rubber & Chemical - Inward inspection - Rubber Mixing - Hardness inspection - Moulding - Visual inspection - Standard packing & Dispatch. |
4. Process Details
Process / Operation | Rubber Moulding |
Outsource | No |
Machine / Cell | Moulding |
Machine / Cell No. | Moulding |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Less or more temperature | PLC control / Machine stop if parameter not okay | O |
Material | Wrong material used | We have checked hardness data last six month & found okay | O |
Tool | Mould tool not okay | Mould leakage | X |
Machine | Less or more curing time . | PLC control / Machine stop if parameter not okay | O |
Man | Skipped from inspection . | NG parts found at customer End . | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 4000 |
7. Root Cause Analysis (Occurance)
Why 1 | During deflashing operation . |
Why 2 | Difficult to deflashing due to thick flash |
Why 3 | Material flow not uniform due to mould leakage . |
Why 4 | Mold parallelism not okay . |
Why 5 | Mold tool PM frequency is Less . |
Root Cause (Occurance) | Mold tool PM frequency is Less . |
Root Cause Analysis (Outflow)
Why 1 | Flash & cut mark on part . |
Why 2 | NG part found at customer end . |
Why 3 | Inspector not aware . |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Inspector not aware . |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | Training & awareness given to inspector. OPL display at inspection stage . | Mr Amar | 15/10/2022 | 14/10/2022 | Completed |
Occurance | Mould PM frequency Increase . | Mr Ravi | 11/10/2022 | 11/10/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Visual inspection . |
Inspection Method | Other |
Other Inspection Method | Visual inspection |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 4000 |
10. Evidance of Countermeasure
Occurance (Before) |
Mould Leakage . 298_Occurance_Before.pdf |
Occurance (After) |
Blue matching done & mould parallelism found okay.
Mould PM frequency Increase from 7000 shots to 5000 Shots . 298_Occurance_After.pdf |
Outflow (Before) |
inspector not aware . 298_Outflow_Before.pdf |
Outflow (After) |
Training & awareness given to inspector.
OPL display at inspection stage. 298_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Applicable for all Bumps stop parts . |
12. Document Review
Documents | InspCheckSheet |
Specify Other Document | N/A |
13. Effectiveness Of Action
Reviewed Quantity | 1 |
Reason for submission | Found OK |