QFR No - 7000923409
Defect Details
NC No. 7000923409
NC Date 19/06/2023
NC Submission Date
Part No. S2AB00512B
Part Name ADJUSTER PLATED
Supplier Name & Code 100782-NICE STEEL INDUSTRIES
ETL Plant 1143-ETL Suspension Halol, Vadodara
Defect Details PAINT PEEL OFF-platting peel off
 
1. Problem Description
Defect Description Plating peel off
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 64
Is Defect Repeatative? Yes
Defect Sketch / Photo rg1cdvhmffno3if32xkq3udb.jpg
Supplier Communication Details
Quality Head Email ID ppc.nice@batragroup.biz
Plant Head/CEO Email ID ho.nice@batragroup.biz
MD Email ID hitesh@batragroup.biz
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
0
0
2000
0
3000
Check Qty
1000
0
0
2000
0
3000
NG Qty
0
0
0
1
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
All part visual inspection done
 
3. Process Flow
Process Flow Description
10 RECEIVING INSPECTION 20 STORAGE 30 BLANKING 40 1st BENDING ( `U` BENDING) 50 FINAL BENDING ( ROUNDING ) 60 MIG WELDING 70 FLAIRING 80 ID SIZING 90 SIDE GRINDING 100 BROACHING 110 SINGLE GROOVE MATCHING 120 HEAD GRINDING 130 OUTSIDE MOVEMENT FOR PLATING 140 STORAGE & RQC INSP. OF PLATED MATERIAL 150 FINAL INSPECTION 160 PACKING & DISPATCH TO CUSTOMER
 
4. Process Details
Process / Operation PLATING
Outsource Yes
Machine / Cell PLATING PROCESS
Machine / Cell No. HANGER
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodHANGER INSPECTIONHANGER MAINTENANCE DONE ON MONTHLY BASIS BUT INSPECTION FREQUENCY WAS NOT DEFINEDO
ManUNSKILL MANPOWERSKILL MATRIX AVAILABLEX
ToolHANGER CONDITION WAS OKCHECK AND FOUND HANGER HOOK DAMAGEO
MachineMACHINE CAPACITY WAS LOWFOUND OKX
MaterialWRONG CHEMICAL USEDMTC VERFIFIED WITH TECHNICAL DATA SHEETX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method VISUAL
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 PLATING LAYER WAS DAMAGE IN PART
Why 2 CHROME PLATING NOT DONE AS REQUIERD
Why 3 CURRENT FLOW WAS NOT REGULAR
Why 4 HANGER HOOKS WAS DAMAGE
Why 5 NO DAILY HANGER INSPECTION SYSTEM WAS AVAILABLE ,ONLY HANGER MAINTENANCE DONE
Root Cause (Occurance) 1-HANGER HOOKS WAS DAMAGE 2-NO DAILY HANGER INSPECTION SYSTEM WAS AVAILABLE ,ONLY HANGER MAINTENANCE DONE
 
Root Cause Analysis (Outflow)
Why 1 DEFECTIVE PART FOUND AT CUSTOMER END
Why 2 PARTS NOT DOUND DURING VISUAL INSPECTION
Why 3
Why 4
Why 5
Root Cause (Outflow) PARTS NOT DOUND DURING VISUAL INSPECTION
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceWEEKLY HANGER INSPECTION STARTEDVEEKAY IND.28/06/202325/06/2023Completed
OccuranceHANGER INSPECTION CHECKSHEET MADE AND FOLLOWEDVEEKAY27/06/202325/06/2023Completed
Outflow200% VISUAL INSPECTION STARTEDNICE26/06/202325/06/2023Completed
OutflowQUALITY GATE IMPLEMENTEDNICE STEEL26/06/202325/06/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 200% VISUAL STARTED
Inspection Method Other
Other Inspection Method VISUAL
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size VISUAL
10. Evidance of Countermeasure
Occurance (Before) NO DAILY CHECKPOINT
486_Occurance_Before.pdf
Occurance (After) DAILY CHECKPOINT UPADTED
486_Occurance_After.xlsx
Outflow (Before) OPL
486_Outflow_Before.pdf
Outflow (After) OPL & TRAINING
486_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant HANGER MONITORING STARTED FOR OTHER PARTS
 
12. Document Review
Documents JHCheckSheet
Specify Other Document DAILY CHECKSHEET
 
13. Effectiveness Of Action
Reviewed Quantity 500
Reason for submission ok