QFR No - 7000939009
Defect Details
NC No. | 7000939009 |
NC Date | 23/08/2023 |
NC Submission Date | |
Part No. | 520FN02602 |
Part Name | CLUTCH HOLDER (C20002) |
Supplier Name & Code | 101067-MEGA METALS |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | EXTRA METAL-Extra metrial 1cavity & Heat check |
1. Problem Description
Defect Description | Extra Material at Bolt resting face-Fitment issue |
Detection Stage | Receipt |
Problem Severity | Fitment |
NG Quantity | 1200 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | mukesh.pathak@megametalsindia.com |
Plant Head/CEO Email ID | lalit.goel@megametalsindia.com |
MD Email ID | raman.arora@megametalsindia.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
1000
|
2000
|
0
|
500
|
2000
|
5500
|
Check Qty |
1000
|
2000
|
0
|
500
|
2000
|
5500
|
NG Qty |
250
|
500
|
0
|
5
|
0
|
755
|
Scrap | 5 |
Rework | 750 |
Under Deviation | 0 |
Containment Action |
---|
Defected lot quarantine, segregated and reworked ETL Stock as well as Mega Metals stock |
3. Process Flow
Process Flow Description |
---|
PDC , Fettling, Machining, Final Inspection, PDIR, Dispatch |
4. Process Details
Process / Operation | PDC |
Outsource | No |
Machine / Cell | PDC |
Machine / Cell No. | HPDC-04 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Slipped from inspection | WI Checked and Verified with Inspectors | O |
Tool | Heat Crack in die at C1Cavity at specific area | Verification done insert found the minor heat crack in die | O |
Method | Could not removed in fettling | It was not pre decided /was not in WI | O |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | Visual Inspection |
Check Point at Final Inspection | No |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Extra metal on clutch holder |
Why 2 | Due to dent in die. |
Why 3 | Dent occurred during the removing stucked flash |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Dent occurred during the removing stucked flash. |
Root Cause Analysis (Outflow)
Why 1 | Extra metal on clutch holder |
Why 2 | Part slipped from final inspection |
Why 3 | Because check point not available in WI. |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Because check point not available in WI. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | laser welding done | suresh | 15/12/2023 | 01/09/2023 | Completed |
Outflow | WI revise | Rajesh | 16/12/2023 | 30/08/2023 | Completed |
Outflow | training provided to all inspectors | Rajesh | 15/12/2023 | 04/09/2023 | Completed |
Occurance | training provided to all operators | Arun kumar | 15/12/2023 | 04/09/2023 | Completed |
Outflow | Quality alert displayed on final inspection table | Subhash kumar | 30/08/2023 | 30/08/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | check point added |
Inspection Method | Other |
Other Inspection Method | visual |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Quality Alert -Before condition picture 530_Occurance_Before.pdf |
Occurance (After) |
OJT 530_Occurance_After.pdf |
Outflow (Before) |
Before After of WI
Before WI 530_Outflow_Before.pdf |
Outflow (After) |
Revised WI 530_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | No |
Applicable Machine / Model / Plant | Only one Part running at our end |
12. Document Review
Documents | PFMEA, WISOP |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |