QFR No - 7000939009
Defect Details
NC No. 7000939009
NC Date 23/08/2023
NC Submission Date
Part No. 520FN02602
Part Name CLUTCH HOLDER (C20002)
Supplier Name & Code 101067-MEGA METALS
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details EXTRA METAL-Extra metrial 1cavity & Heat check
 
1. Problem Description
Defect Description Extra Material at Bolt resting face-Fitment issue
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 1200
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID mukesh.pathak@megametalsindia.com
Plant Head/CEO Email ID lalit.goel@megametalsindia.com
MD Email ID raman.arora@megametalsindia.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1000
2000
0
500
2000
5500
Check Qty
1000
2000
0
500
2000
5500
NG Qty
250
500
0
5
0
755
 
Scrap 5
Rework 750
Under Deviation 0
Containment Action
Defected lot quarantine, segregated and reworked ETL Stock as well as Mega Metals stock
 
3. Process Flow
Process Flow Description
PDC , Fettling, Machining, Final Inspection, PDIR, Dispatch
 
4. Process Details
Process / Operation PDC
Outsource No
Machine / Cell PDC
Machine / Cell No. HPDC-04
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManSlipped from inspectionWI Checked and Verified with InspectorsO
ToolHeat Crack in die at C1Cavity at specific areaVerification done insert found the minor heat crack in dieO
MethodCould not removed in fettlingIt was not pre decided /was not in WIO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual Inspection
Check Point at Final Inspection No
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Extra metal on clutch holder
Why 2 Due to dent in die.
Why 3 Dent occurred during the removing stucked flash
Why 4
Why 5
Root Cause (Occurance) Dent occurred during the removing stucked flash.
 
Root Cause Analysis (Outflow)
Why 1 Extra metal on clutch holder
Why 2 Part slipped from final inspection
Why 3 Because check point not available in WI.
Why 4
Why 5
Root Cause (Outflow) Because check point not available in WI.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurancelaser welding donesuresh15/12/202301/09/2023Completed
OutflowWI reviseRajesh16/12/202330/08/2023Completed
Outflowtraining provided to all inspectorsRajesh15/12/202304/09/2023Completed
Occurancetraining provided to all operatorsArun kumar15/12/202304/09/2023Completed
OutflowQuality alert displayed on final inspection tableSubhash kumar30/08/202330/08/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details check point added
Inspection Method Other
Other Inspection Method visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Quality Alert -Before condition picture
530_Occurance_Before.pdf
Occurance (After) OJT
530_Occurance_After.pdf
Outflow (Before) Before After of WI Before WI
530_Outflow_Before.pdf
Outflow (After) Revised WI
530_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant Only one Part running at our end
 
12. Document Review
Documents PFMEA, WISOP
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission