QFR No - 7000939452
Defect Details
NC No. 7000939452
NC Date 23/08/2023
NC Submission Date
Part No. C3CE00201B
Part Name CLUTCH SHAFT ASSLY
Supplier Name & Code 100264-SAI INDUSTRIES
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details CRACKS-flairing dia obs 4.26 & flange cracked
 
1. Problem Description
Defect Description Crack observed at flaring dia -During Riveting
Detection Stage Inprocess
Problem Severity Function
NG Quantity 2
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID info@sai-industries.com
Plant Head/CEO Email ID info@sai-industries.com
MD Email ID umesh.honap@gmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
200
480
0
280
0
960
Check Qty
200
480
0
280
0
960
NG Qty
2
0
0
0
0
2
 
Scrap 2
Rework 0
Under Deviation 0
Containment Action
In ETL stock verified 200 Nos. found 2 nos cracks in Assly line. In A`Bad Warehouse stock verified 480 Nos.found no any cracks . InSai Inhouse stock verified 288 Nos.found no anycracks . All riveting parameter checked found ok except rivet height. Clutch Flange Bend/Warpage above 0.30mm. CNC Facing operation all parameters found ok.
 
3. Process Flow
Process Flow Description
Rivetting
 
4. Process Details
Process / Operation Rivetting
Outsource No
Machine / Cell Assly
Machine / Cell No. Rivetting
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MaterialClutch Flange bend/warpage above 0.30mm or may be internal crack in casting.Parallerity not ok observed.O
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Dial & Fixture
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Why 1:-CRACKS-flairing dia obs 4.26 & flange cracked
Why 2 Why 2:- Rivetting operation, Rivet height uneven or excess.
Why 3 Why 3:- Clutch Flange parallerity above 0.30mm.
Why 4 Why 4:- Clutch Flange bend/warpage above 0.30mm or may be internal crack in casting. Already informed to ETL time to time refer mail and rejection returned also.
Why 5
Root Cause (Occurance) Clutch Flange bend/warpage above 0.30mm or may be internal crack in casting. Already informed to ETL time to time refer mail and rejection returned also.
 
Root Cause Analysis (Outflow)
Why 1 Why 1:-CRACKS-flairing dia obs 4.26 & flange cracked
Why 2 Why 2:- Not proper adreesed in 100% visual inspection.
Why 3 Why 3:- Not kept crack assly in rejection bin.
Why 4 why 4:- Cracks assly may be mix up in ok assly.
Why 5
Root Cause (Outflow) Cracks assly may be mix up in ok assly.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
Occurance1) ETL will ensure defect free(without bend/warpage)clutch flange supplied to Sai. 2) Received all clutch flange segrrigate for parallerity and Only Ok flange used for assly. 3) For crack free parts rivet height to be increased by 0.20mm.i.e.within 0.70mm and ETL will give approval for increase the the same.ETL and SAI02/09/202302/10/2023Completed
Outflow2) After 100% visual inspection marked Blue dot as identification.SAI01/09/202301/09/2023Completed
Outflow1) Display Ok and Not ok photo in final/visual inspection stage.SAI01/09/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Firewall inspection started.
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) No Parameter in SOP
531_Occurance_Before.pdf
Occurance (After) Add parameter in SOP
531_Occurance_After.pdf
Outflow (Before) Not Display Photo
531_Outflow_Before.pdf
Outflow (After) Display Photo
531_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Clutch Shaft Assly BS III and BS VI PVPL
 
12. Document Review
Documents WISOP
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission OK