QFR No - 7000943532
Defect Details
NC No. 7000943532
NC Date 11/09/2023
NC Submission Date
Part No. C30400101B
Part Name GEAR PRIMARY ASSLY
Supplier Name & Code 100237-SANJEEV AUTO PARTS MRFS PVT LT
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details HIGHT U/SIZE.-rusty issue & boss hight obs 24.03 mm
 
1. Problem Description
Defect Description Boss Height found undersize up to 24.03~24.07 mm against 24.10~24.20 mm
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 7
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID vpwankhade@sanjeevgroup.com
Plant Head/CEO Email ID rmtiwari@sanjeevgroup.com
MD Email ID maithilee@sanjeevgroup.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1280
0
0
300
270
1850
Check Qty
1280
0
0
300
270
1850
NG Qty
513
0
0
11
6
530
 
Scrap 0
Rework 17
Under Deviation 0
Containment Action
Cleaning done & 100% inspection done for suspected defective batch
 
3. Process Flow
Process Flow Description
Sn Process Flow 1 Raw Material Inward 2 Bar Cutting 3 Billet Heating 4 Hot Forging 5 Normalizing 6 Shotblasting 7 Coining 8 Preturning 9 Peircing-1 10 Peircing-2 11 Shaving-1 12 Shaving-2 13 Milling-1 14 Milling-2 15 Finish turning 1st setup 16 Finish turning 2nd setup 17 Finish turning 3rd setup 18 Deburring 19 Final Inspection CNC Blank 20 Inward Inspection CNC Blank 21 Traciability Marking 22 Hobbing 23 Teeth Chamfering 24 Gear Shaving 25 Heat tratment 26 Shotblasting 27 ID Turning 28 Bush Pressing 29 Bush Turning 30 Washing 31 Final inspection 32 Dispatch
 
4. Process Details
Process / Operation Shot blasting
Outsource No
Machine / Cell Heat treatment
Machine / Cell No. HT/Shot blasting
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineDust & Moisture in shotsDust & Moisture in shotsX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual inspection
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 20 / lot
7. Root Cause Analysis (Occurance)
Why 1 Rusty issue / rusty spots observed on parts
Why 2 Parts observed uncleaned after shot blasting
Why 3 Excess dust and moisture in shots
Why 4 Shots screening freqency not followed
Why 5
Root Cause (Occurance) Shots screening freqency not followed
 
Root Cause Analysis (Outflow)
Why 1 Rusty issue / rusty spots observed on parts
Why 2 Parts observed uncleaned after shot blasting
Why 3 Skipped from inspection
Why 4 Sample inspection
Why 5
Root Cause (Outflow) Sample inspection
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceShots cleaning / screening doneMr. Shelke15/09/2023Completed
Outflow100% visual inspectionvpw12/09/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100 % visual inspection & sample millipore inspection
Inspection Method Other
Other Inspection Method Visual & millipore i
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Moisture & dust in shots
547_Occurance_Before.pdf
Occurance (After) Moisture & dust removed by shot screening & dosing lime powder
547_Occurance_After.pdf
Outflow (Before) No check point for rust
547_Outflow_Before.pdf
Outflow (After) Check point added to check rusty part
547_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant GPH all models
 
12. Document Review
Documents WISOP, InspCheckSheet
Specify Other Document WI eye sequence char
 
13. Effectiveness Of Action
Reviewed Quantity 500
Reason for submission OK