QFR No - 7000951769
Defect Details
NC No. 7000951769
NC Date 11/10/2023
NC Submission Date
Part No. F1DZ00902B
Part Name FORK BOLT K86A
Supplier Name & Code 101037-SHREE PATEL INDUSTRIES
ETL Plant 1136-ETL Suspension Sanand
Defect Details MATERIAL DEFECT-Material Defect on OD
 
1. Problem Description
Defect Description Material defect found on head (OD) of fork bolt K86
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 980
Is Defect Repeatative? No
Defect Sketch / Photo ekltmoemj1irgygxc21udo1u.jpg
Supplier Communication Details
Quality Head Email ID quality_spi@rediffmail.com
Plant Head/CEO Email ID planthead_spi@rediffmail.com
MD Email ID rspatel_spi@rediffmail.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
6000
0
0
0
0
6000
Check Qty
6000
0
0
0
0
6000
NG Qty
1
0
0
0
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
All suspected part checked and rejected part scraped.
 
3. Process Flow
Process Flow Description
10.Incoming 20.Traub Turning 30.CNC 1st Setup 40.CNC 2nd Setup 50.Plating 60.Inspection 70.Packing & Dispatch
 
4. Process Details
Process / Operation Incoming
Outsource Yes
Machine / Cell Incoming (INWARD)
Machine / Cell No. RM INWARD
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodImproper material handlingDuring genba visit, We found that input and output material are stored on difined location.O
MachinePower failure during operationBy verification power failure register, all the part between power failure are kept in hold area foO
MachineImproper alignment of MachineBy verification of PM check sheet, Machine alignment found okO
ManUnskilled manpowerSkill matrix verified and all the manpower found on required level 2 and level 3O
MaterialNG incoming materiaDuring Gemba visit, We found all incoming material ok as per specification but visually damage.X
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method VISUAL
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size 25:1
7. Root Cause Analysis (Occurance)
Why 1 Defective part reached at custommer end.
Why 2 This type of defect generated during CNC turning.
Why 3 Operator not done visual Inspection during process.
Why 4 Checking Frequency not defined.
Why 5
Root Cause (Occurance) 1_ These Types of material defcet not visible during incoming inspection 2_These types of defect generated after CNC turning process But During process part not checked by Operator & Due to this defective part not captured during process .
 
Root Cause Analysis (Outflow)
Why 1 Defective part reached at custommer end.
Why 2 Part not captured during final inspection.
Why 3 Inspector not aware about this type of defect.
Why 4 Training not provided to inspector for related defect.
Why 5
Root Cause (Outflow) Due to inspector lack of defect awarness.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceChecking frequency define at machining during process.Sanjay Lakhatariya15/10/202315/10/2023Completed
OutflowTraining provided to inspector for related defect. Defect sample displayed for better understandingSanjay Lakhatariya15/10/202315/10/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details NO
Inspection Method Other
Other Inspection Method VISUAL
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Control Plan
571_Occurance_Before.xlsx
Occurance (After) Control plan part checking frequency add in CNC 1st and CNC 2nd Turning.
571_Occurance_After.xlsx
Outflow (Before) Defect sample not displayed
571_Outflow_Before.jpeg
Outflow (After) Training provided to concern person
571_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Fork bolt K86A
 
12. Document Review
Documents ControlPlan
Specify Other Document TRAINING RECORD
 
13. Effectiveness Of Action
Reviewed Quantity 5
Reason for submission Material defect on head of fork bolt