QFR No - 7000951769
Defect Details
NC No. | 7000951769 |
NC Date | 11/10/2023 |
NC Submission Date | |
Part No. | F1DZ00902B |
Part Name | FORK BOLT K86A |
Supplier Name & Code | 101037-SHREE PATEL INDUSTRIES |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | MATERIAL DEFECT-Material Defect on OD |
1. Problem Description
Defect Description | Material defect found on head (OD) of fork bolt K86 |
Detection Stage | Receipt |
Problem Severity | Aesthetic |
NG Quantity | 980 |
Is Defect Repeatative? | No |
Defect Sketch / Photo | ekltmoemj1irgygxc21udo1u.jpg |
Supplier Communication Details
Quality Head Email ID | quality_spi@rediffmail.com |
Plant Head/CEO Email ID | planthead_spi@rediffmail.com |
MD Email ID | rspatel_spi@rediffmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
6000
|
0
|
0
|
0
|
0
|
6000
|
Check Qty |
6000
|
0
|
0
|
0
|
0
|
6000
|
NG Qty |
1
|
0
|
0
|
0
|
0
|
1
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All suspected part checked and rejected part scraped. |
3. Process Flow
Process Flow Description |
---|
10.Incoming 20.Traub Turning 30.CNC 1st Setup 40.CNC 2nd Setup 50.Plating 60.Inspection 70.Packing & Dispatch |
4. Process Details
Process / Operation | Incoming |
Outsource | Yes |
Machine / Cell | Incoming (INWARD) |
Machine / Cell No. | RM INWARD |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Method | Improper material handling | During genba visit, We found that input and output material are stored on difined location. | O |
Machine | Power failure during operation | By verification power failure register, all the part between power failure are kept in hold area fo | O |
Machine | Improper alignment of Machine | By verification of PM check sheet, Machine alignment found ok | O |
Man | Unskilled manpower | Skill matrix verified and all the manpower found on required level 2 and level 3 | O |
Material | NG incoming materia | During Gemba visit, We found all incoming material ok as per specification but visually damage. | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | VISUAL |
Check Point at Final Inspection | No |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 25:1 |
7. Root Cause Analysis (Occurance)
Why 1 | Defective part reached at custommer end. |
Why 2 | This type of defect generated during CNC turning. |
Why 3 | Operator not done visual Inspection during process. |
Why 4 | Checking Frequency not defined. |
Why 5 | |
Root Cause (Occurance) | 1_ These Types of material defcet not visible during incoming inspection 2_These types of defect generated after CNC turning process But During process part not checked by Operator & Due to this defective part not captured during process . |
Root Cause Analysis (Outflow)
Why 1 | Defective part reached at custommer end. |
Why 2 | Part not captured during final inspection. |
Why 3 | Inspector not aware about this type of defect. |
Why 4 | Training not provided to inspector for related defect. |
Why 5 | |
Root Cause (Outflow) | Due to inspector lack of defect awarness. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Checking frequency define at machining during process. | Sanjay Lakhatariya | 15/10/2023 | 15/10/2023 | Completed |
Outflow | Training provided to inspector for related defect. Defect sample displayed for better understanding | Sanjay Lakhatariya | 15/10/2023 | 15/10/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | NO |
Inspection Method | Other |
Other Inspection Method | VISUAL |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Control Plan 571_Occurance_Before.xlsx |
Occurance (After) |
Control plan part checking frequency add in CNC 1st and CNC 2nd Turning. 571_Occurance_After.xlsx |
Outflow (Before) |
Defect sample not displayed 571_Outflow_Before.jpeg |
Outflow (After) |
Training provided to concern person 571_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Fork bolt K86A |
12. Document Review
Documents | ControlPlan |
Specify Other Document | TRAINING RECORD |
13. Effectiveness Of Action
Reviewed Quantity | 5 |
Reason for submission | Material defect on head of fork bolt |