QFR No - 7000987844
Defect Details
NC No. | 7000987844 |
NC Date | 20/02/2024 |
NC Submission Date | |
Part No. | 520JT05102 |
Part Name | PLATE CLUTCH PIAGGIO |
Supplier Name & Code | 101138-HINDUSTAN PRESSINGS PVT.LTD. |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | CRACK-Crack issue |
1. Problem Description
Defect Description | Plate Clutch observed Crack |
Detection Stage | Inprocess |
Problem Severity | Function |
NG Quantity | 3900 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo | odwx25kgwj1e0posgteq0nl2.jpg |
Supplier Communication Details
Quality Head Email ID | quality.p1@hpplindia.com |
Plant Head/CEO Email ID | spatil@hpplindia.com |
MD Email ID | rakesh@hpplindia.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
3900
|
0
|
0
|
0
|
0
|
3900
|
Check Qty |
3900
|
0
|
0
|
0
|
0
|
3900
|
NG Qty |
88
|
0
|
0
|
0
|
0
|
88
|
Scrap | 88 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
We have imidiate action check for crack and NG parts segragation done. |
3. Process Flow
Process Flow Description |
---|
RM - Blanking/Piercing - Sandering - Nitriding - Dishing - Final Inspection - Packing |
4. Process Details
Process / Operation | Dishing |
Outsource | No |
Machine / Cell | PP 17 |
Machine / Cell No. | 110T |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | FINAL INSPECTION NOT CHECKE DPROPPELY | INSPECTOR CHECKED IN GAUGE AFTER REWOK JOB | X |
Method | REWOK JOB NOT PROPERLY DONE | EXCESS PRESSURE GIVEN ON PART OBSERVED IN VISUAL DEFECT | X |
6. Inspection Method Analysis (Current)
Inspection Method | Other |
Other Inspection Method | ViSUAL INSPECTION |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | LOT SIZE |
7. Root Cause Analysis (Occurance)
Why 1 | Crack found |
Why 2 | Parts gets excess pressure during staraightning process |
Why 3 | Rework parts (Go gauge not Ok) passing through process |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Rewok Parts (Go Gauge not Ok) passing througth Straigjtning proces |
Root Cause Analysis (Outflow)
Why 1 | Crack found |
Why 2 | 100% inspection done ok parts.In rework parts check visual inspection |
Why 3 | Inspector aware about the checking hair line crack in rework parts. |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | Inspector aware about the checking hair line crack in rework parts. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | WI for the rework parts (Go gauge not Ok) passed throught straightning and check parts visualyy by 100% and parts indetified seperatly | Mr. Hitendra Patil(HPPL) and Mr, Kiran(HPPL) | 07/03/2024 | 09/03/2024 | Completed |
Occurance | Traininh give to supervisor and opearartor to rework procedure. | Mr. Hitendra Patil(HPPL) and Mr, Kiran(HPPL) | 07/03/2024 | 09/03/2024 | Completed |
Outflow | 1. Inspector training regarding all final inspection of rework job by 100% 2. 100% checked the gauge passing throught plates and varify the experienced senior QA person for next 3 lot | Mr.Kiran ( HPPL | 12/03/2024 | 13/03/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | REWORK PARTS VISUAL INSPECTION DONE AS PER WORK INSTRUCTION. |
Inspection Method | Other |
Other Inspection Method | VISUAL |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | LOT SIZE |
10. Evidance of Countermeasure
Occurance (Before) |
Work instruction not avilable 687_Occurance_Before.pdf |
Occurance (After) |
We have training given to opearator as per work instruction 687_Occurance_After.pdf |
Outflow (Before) |
Check job visually not q alerat avilable 687_Outflow_Before.pdf |
Outflow (After) |
Q alert display on finl inspection 687_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All parts |
12. Document Review
Documents | ControlPlan, PFMEA, WISOP |
Specify Other Document | NO |
13. Effectiveness Of Action
Reviewed Quantity | 1000 |
Reason for submission | OK |