QFR No - 7001010242
Defect Details
NC No. 7001010242
NC Date 01/05/2024
NC Submission Date
Part No. F2FA19033M
Part Name K0PG FORK PIPE MACHINED
Supplier Name & Code 101109-TUBE INVESTMENTS OF INDIA LIMI
ETL Plant 1136-ETL Suspension Sanand
Defect Details RUN OUT MORE-ID Runout NG and Bend Part
 
1. Problem Description
Defect Description Fork pipe straightness was Observed 0.150 ~0.200 mm against specification 0.06/200 mm. Runout observed was 0.150~0.180 mm against specification 0.08 B.
Detection Stage Inprocess
Problem Severity Function
NG Quantity 765
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID anandms@tii.murugappa.com
Plant Head/CEO Email ID girisha@tii.murugappa.com
MD Email ID mukeshahuja@tii.murugappa.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
3000
0
0
1500
28000
32500
Check Qty
3000
0
0
1500
28000
32500
NG Qty
765
0
0
5
35
805
 
Scrap 805
Rework 0
Under Deviation 0
Containment Action
100% inspection after Rough Grinding at ETL end & 100 % Visual Inspection for Tube Machining OD Chamfer at Final Inspection & Sampling Inspection on Fixture with Dial stand & magnetic Block at Sanand Machining center.
 
3. Process Flow
Process Flow Description
TUBE FORMING - ANNEALING - WET PROCESS - PUSH POINTING - DRAWING - STRESS RELIEVING - STRAIGHTENING - ECT - CTL - FACING & CHAMFERING - FINAL INSPECTION - PACKING
 
4. Process Details
Process / Operation STRAIGHTENING
Outsource No
Machine / Cell TFF straightening machine
Machine / Cell No. TFF straightening mc
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManOperator failed to inspectAuto counted inspected part is match with packed qty so, there is no possibility of failure.O
MachineStraightening roll damageRoll condition verified , no mark observed & no roll change activity done.O
ToolChecking instrument ErrorCalibrated instrument used & the least count 0.01mm so, there is no possibility of instrument error.O
MethodGauge checking Method ErrorOk & NG part checked in existing checking method- Arrived KAPPA is 0.40 so, present checking methodX
MachineStraightening pressure roll reversedStraightening pressure roll bit reversed while straightening process.X
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Fork pipe straightness was Observed 0.150 ~0.200 mm against specification 0.06/200 mm.
Why 2 Straightening pressure roll reversed
Why 3 Straightening Pressure roll partially loosen
Why 4 Pressure roll clamping inherent seal loosened while operation
Why 5 Operator failed lock the inherent seal once in a week.
Root Cause (Occurance) Operator failed lock the inherent seal once in a week.
 
Root Cause Analysis (Outflow)
Why 1 Fork pipe straightness was Observed 0.150 ~0.200 mm against specification 0.06/200 mm.
Why 2 Gauge checking Method Error.
Why 3 Arrived KAPPA is 0.40 after attribute MSA.
Why 4 NG parts are accepted by all appraiser
Why 5 Present run out rest spot & dial indicator not detected corner run out.
Root Cause (Outflow) Present run out rest spot & dial indicator not detected corner run out.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowAdditional one dial indicator added at the both end corner of tube to checking run out.Mr. Satish08/05/202404/05/2024Completed
OccuranceRoll locking mechanism additionally provided outer side of roll adjustment handle.Mr. Satish.13/05/202408/05/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Additional one dial indicator added at the both end corner of tube to checking run out.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100
10. Evidance of Countermeasure
Occurance (Before) Roll locking mechanism not available to roll adjustment handle.
771_Occurance_Before.pptx
Occurance (After) Roll locking mechanism additionally provided outer side of roll adjustment handle.
771_Occurance_After.pptx
Outflow (Before) Bend checking with Dial indicator at middle only.
771_Outflow_Before.pptx
Outflow (After) Three dial indicator , especially added one dial at both end of tube to check tube corner bend also
771_Outflow_After.pptx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Action to be implemented between 280 mm to 305 mm cut length.
 
12. Document Review
Documents WISOP
Specify Other Document NO
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission