QFR No - 7001010242
Defect Details
NC No. | 7001010242 |
NC Date | 01/05/2024 |
NC Submission Date | |
Part No. | F2FA19033M |
Part Name | K0PG FORK PIPE MACHINED |
Supplier Name & Code | 101109-TUBE INVESTMENTS OF INDIA LIMI |
ETL Plant | 1136-ETL Suspension Sanand |
Defect Details | RUN OUT MORE-ID Runout NG and Bend Part |
1. Problem Description
Defect Description | Fork pipe straightness was Observed 0.150 ~0.200 mm against specification 0.06/200 mm. Runout observed was 0.150~0.180 mm against specification 0.08 B. |
Detection Stage | Inprocess |
Problem Severity | Function |
NG Quantity | 765 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | anandms@tii.murugappa.com |
Plant Head/CEO Email ID | girisha@tii.murugappa.com |
MD Email ID | mukeshahuja@tii.murugappa.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
3000
|
0
|
0
|
1500
|
28000
|
32500
|
Check Qty |
3000
|
0
|
0
|
1500
|
28000
|
32500
|
NG Qty |
765
|
0
|
0
|
5
|
35
|
805
|
Scrap | 805 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% inspection after Rough Grinding at ETL end & 100 % Visual Inspection for Tube Machining OD Chamfer at Final Inspection & Sampling Inspection on Fixture with Dial stand & magnetic Block at Sanand Machining center. |
3. Process Flow
Process Flow Description |
---|
TUBE FORMING - ANNEALING - WET PROCESS - PUSH POINTING - DRAWING - STRESS RELIEVING - STRAIGHTENING - ECT - CTL - FACING & CHAMFERING - FINAL INSPECTION - PACKING |
4. Process Details
Process / Operation | STRAIGHTENING |
Outsource | No |
Machine / Cell | TFF straightening machine |
Machine / Cell No. | TFF straightening mc |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Operator failed to inspect | Auto counted inspected part is match with packed qty so, there is no possibility of failure. | O |
Machine | Straightening roll damage | Roll condition verified , no mark observed & no roll change activity done. | O |
Tool | Checking instrument Error | Calibrated instrument used & the least count 0.01mm so, there is no possibility of instrument error. | O |
Method | Gauge checking Method Error | Ok & NG part checked in existing checking method- Arrived KAPPA is 0.40 so, present checking method | X |
Machine | Straightening pressure roll reversed | Straightening pressure roll bit reversed while straightening process. | X |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Fork pipe straightness was Observed 0.150 ~0.200 mm against specification 0.06/200 mm. |
Why 2 | Straightening pressure roll reversed |
Why 3 | Straightening Pressure roll partially loosen |
Why 4 | Pressure roll clamping inherent seal loosened while operation |
Why 5 | Operator failed lock the inherent seal once in a week. |
Root Cause (Occurance) | Operator failed lock the inherent seal once in a week. |
Root Cause Analysis (Outflow)
Why 1 | Fork pipe straightness was Observed 0.150 ~0.200 mm against specification 0.06/200 mm. |
Why 2 | Gauge checking Method Error. |
Why 3 | Arrived KAPPA is 0.40 after attribute MSA. |
Why 4 | NG parts are accepted by all appraiser |
Why 5 | Present run out rest spot & dial indicator not detected corner run out. |
Root Cause (Outflow) | Present run out rest spot & dial indicator not detected corner run out. |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Outflow | Additional one dial indicator added at the both end corner of tube to checking run out. | Mr. Satish | 08/05/2024 | 04/05/2024 | Completed |
Occurance | Roll locking mechanism additionally provided outer side of roll adjustment handle. | Mr. Satish. | 13/05/2024 | 08/05/2024 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Additional one dial indicator added at the both end corner of tube to checking run out. |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100 |
10. Evidance of Countermeasure
Occurance (Before) |
Roll locking mechanism not available to roll adjustment handle. 771_Occurance_Before.pptx |
Occurance (After) |
Roll locking mechanism additionally provided outer side of roll adjustment handle. 771_Occurance_After.pptx |
Outflow (Before) |
Bend checking with Dial indicator at middle only. 771_Outflow_Before.pptx |
Outflow (After) |
Three dial indicator , especially added one dial at both end of tube to check tube corner bend also 771_Outflow_After.pptx |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Action to be implemented between 280 mm to 305 mm cut length. |
12. Document Review
Documents | WISOP |
Specify Other Document | NO |
13. Effectiveness Of Action
Reviewed Quantity | |
Reason for submission |