QFR No - 7001018333
Defect Details
NC No. 7001018333
NC Date 29/05/2024
NC Submission Date
Part No. F1GN01102B
Part Name MAIN SPRING K86A
Supplier Name & Code 100186-SAGAR SPRINGS PRIVATE LIMITED
ETL Plant 1136-ETL Suspension Sanand
Defect Details THICKNESS UNDERSIZE-End coil tip thickness undersize
 
1. Problem Description
Defect Description End coil thickness found 0.5 mm against specification 0.8 mm (Min).
Detection Stage Receipt
Problem Severity Function
NG Quantity 4000
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@sagarsprings.com
Plant Head/CEO Email ID ajai.singh@sagarsprings.com
MD Email ID sagar@sagarsprings.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
8000
0
0
2000
0
10000
Check Qty
8000
0
0
2000
0
10000
NG Qty
4000
0
0
100
0
4100
 
Scrap 4100
Rework 0
Under Deviation 0
Containment Action
Scrap
 
3. Process Flow
Process Flow Description
COILING,TEMPRING,GRINDING.,SHOT PEENING ,2ND TEMPRING,WAVINESS
 
4. Process Details
Process / Operation Grinding
Outsource No
Machine / Cell Grinding
Machine / Cell No. Grinding Machine
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManUnksilled operator not set machine properly and check it properly result in togeneration of rejectiFound operator deputed are well understood of grinidng process and deffect itcause and counter measO
MaterialWrong grade wheel result on grinding performanceCheck the grade of wheel used ie ceramic wheelO
MethodFaulty program will result into more feed, full grinding, less grinding or tapergrinding in some caCheck the program used for grinding it was found OKO
MethodGrinding angle moreGrinding angle found 300-350deg and tip thickness found less than 0.80 mmX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Sampling
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size Sample Pla
7. Root Cause Analysis (Occurance)
Why 1 Grinding angle more
Why 2 Grinding angle measures 300° to 350° against specification 320° minimum
Why 3 Grinding angle maintained at higher band causing thickness less
Why 4
Why 5
Root Cause (Occurance) Grinding angle maintained at higher band (300° to 350°) causing thickness less
 
Root Cause Analysis (Outflow)
Why 1 Tip thickness less
Why 2 Inspection done on sampling basis
Why 3
Why 4
Why 5
Root Cause (Outflow) Inspection done on sampling basis
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceAt grinding stage grinding angle will be maintained 320deg minimum to maintain tip thickness more than 0.80mmVDP01/06/202401/06/2024Completed
Outflow100% Visual inspection started for grinding angle at grinding stageVDP01/06/202401/06/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details No Change
Inspection Method Other
Other Inspection Method 100% Visual Inspecti
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size sample Pla
10. Evidance of Countermeasure
Occurance (Before) Grinding Angle 300° to 350°
826_Occurance_Before.pdf
Occurance (After) Grinding Angle 320° minimum tip thickness more than 0.80 mm
826_Occurance_After.pdf
Outflow (Before) Sampling Inspection at Grinding stage
826_Outflow_Before.pdf
Outflow (After) 100% Visual Inspection at Grinding stage
826_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant This action is applicable for this spring only.
 
12. Document Review
Documents ControlPlan, PFMEA
Specify Other Document In process Inspectio
 
13. Effectiveness Of Action
Reviewed Quantity 5
Reason for submission Tip thickness found less against specified 0.8 mm min.