QFR No - 7001045639
Defect Details
NC No. 7001045639
NC Date 23/08/2024
NC Submission Date
Part No. S1AB00612B
Part Name ADJUSTER PLATED
Supplier Name & Code 100782-NICE STEEL INDUSTRIES
ETL Plant 1136-ETL Suspension Sanand
Defect Details PLATING NOT OK-Plating thickness NG.
 
1. Problem Description
Defect Description Plating thickness found 4 microns less.
Detection Stage Inprocess
Problem Severity Aesthetic
NG Quantity 5200
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID ppc.nice@batragroup.biz
Plant Head/CEO Email ID ho.nice@batragroup.biz
MD Email ID hitesh@batragroup.biz
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
5200
0
0
1200
0
6400
Check Qty
5200
0
0
1200
0
6400
NG Qty
5200
0
0
1200
0
6400
 
Scrap 0
Rework 6400
Under Deviation 0
Containment Action
Re-plating to done in all parts
 
3. Process Flow
Process Flow Description
10 RECEIVING INSPECTION 20 STORAGE 30 BLANKING 40 1st BENDING ( `U` BENDING) 50 FINAL BENDING ( ROUNDING ) 60 MIG WELDING 70 FLAIRING 1st 80 FLAIRING 2nd 90 ID SIZING 100 SIDE GRINDING & BUFFING 110 REROUNDING 120 BROACHING 130 HEAD GRINDING 140 OUTSIDE MOVEMENT FOR PLATING 150 STORAGE & RQC INSP. OF PLATED MATERIAL 160 FINAL INSPECTION 170 PACKING & DISPATCH
 
4. Process Details
Process / Operation Plating
Outsource Yes
Machine / Cell Auto tank
Machine / Cell No. tank
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineCurrent was not proper flow at Zinc plating tanksChecked and found hanger rustyO
MethodSOP not followedSOP followed and records verifiedX
MaterialWrong chemical usedChemical checked and found okX
MaterialChemical concertation was not okTesting done at internal lab and found okX
MachineBath cleaning tank was not workingChecked and found okX
MachineZinc plating tank was not workingChecked and found okX
MachineHanger hooks was rustyChecked and found NGO
MethodProcess sequence was wrongProcess and and found as per control planX
ManUnskilled manpowerSkill matrix availableX
ToolWrong tank usedFound okX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method VISUAL
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size VISUAL
7. Root Cause Analysis (Occurance)
Why 1 Plating thickness NG in part
Why 2 Plating not done on part as per specification
Why 3 Current was not properly flow on parts during plating
Why 4 Hanger hooks was rusty
Why 5 Zinc carbon was deposited at hanger hooks
Root Cause (Occurance) 1-Zinc carbon was deposited at hanger hooks 2-Hanger hooks was rusty
 
Root Cause Analysis (Outflow)
Why 1 Thickness NG part found at customer end
Why 2 Final inspector not detect the ng part at Final inspection stage
Why 3 PDI inspector check some sample parts during PDI
Why 4 Part not checked 100% for plating thickness at PDI
Why 5 As per sampling plan only sample basis parts checked during PDI
Root Cause (Outflow) PDI inspector check some sample parts during PDI
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceDaily hanger cleaning started instead of weekly maintenanceSupplier25/08/202425/08/2024Completed
Occurance20 spare hanger made for better quality part processSupplier25/08/202425/08/2024Completed
OccuranceSupplier audit check sheet updated and Point will checked by Nice during AuditNice25/08/202425/08/2024Completed
OutflowSampling plan revised and sampling quantity increasedSupplier25/08/202425/08/2024Completed
OutflowSampling plan revised and sampling quantity increased at Nice incomingNice25/08/202425/08/2024Completed
OutflowTraining provided to Final inspector about defectNice & Supplier25/08/202425/08/2024Completed
OccuranceHanger cleaning WI madeSupplier25/08/202425/08/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Sampling plan revised and sampling quantity increased
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 2time
10. Evidance of Countermeasure
Occurance (Before) NA
1037_Occurance_Before.png
Occurance (After) HANGER CLEANING WI
1037_Occurance_After.xlsx
Outflow (Before) NA
1037_Outflow_Before.png
Outflow (After) SAMPLING PLAN SUPPLIER AUDIT REPORT
1037_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents WISOP, JHCheckSheet
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission