QFR No - 7001065590
Defect Details
NC No. 7001065590
NC Date 19/10/2024
NC Submission Date
Part No. S3KJ00202B
Part Name REBOUND STOP
Supplier Name & Code 100990-JAIRAJ ANCILLARIES PVT LTD
ETL Plant 1118-ETL E-92,93 Suspension
Defect Details NOT AS PER SPECIFICATION-I/D STEP SPE=12.50+0.10STPIN 12.50 N.PAS
 
1. Problem Description
Defect Description NOT AS PER SPECIFICATION-I/D STEP SPE=12.50+0.10 STD PIN 12.50 NOT PASS
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 10000
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID planthead.aurangabad@jairajgroup.com
Plant Head/CEO Email ID vp@jairajgroup.com
MD Email ID rajiv@jairajgroup.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
50000
0
0
2500
0
52500
Check Qty
50000
0
0
2500
0
52500
NG Qty
10200
0
0
428
0
10628
 
Scrap 10628
Rework 0
Under Deviation 0
Containment Action
All available material checked 100 % at ETL end and found 10200 no. defective out of 50000 no. checked. All available inhouse FG material checked 100% and found 428 no. defective parts out of 2500 no. checked.
 
3. Process Flow
Process Flow Description
Injection Moulding
 
4. Process Details
Process / Operation Injection Moulding
Outsource No
Machine / Cell Injection Moulding Cell
Machine / Cell No. IMM-01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineOCS & control plan not followed by Machine OperatorVerified as per CP & OCS found ok , as per standard specificationX
ToolMould Cooling Time High/lowChecked with CP & OCS and found OK as per specificationX
MachineBarrel Temperature High/LowChecked with CP & OCS and found OK as per specificationX
MaterialRM Grade not as per CPCheck with MTC & found ok as per specification.X
ManMan Power does not aware about this defect .Slight change in ID shift not identified by Process & final InspectorO
MethodChecking method for OD checkingVerified as per CP/OCS and found checking method adequate for ID/OD CheckingX
ToolMould Cooling Water flow rate at Cooling OutletVerified as per Tool PM checksheet and found as per specificationX
ToolCore & cavity centre not matched.Verified as per tool design and found ID centre shiftO
 
6. Inspection Method Analysis (Current)
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5
7. Root Cause Analysis (Occurance)
Why 1 Defective parts are introduced. (Ie Step in ID )
Why 2 Due to mould core half loose observed with respect to cavity half.
Why 3 Due to one Non operator Guide pin loosen in Core half.
Why 4 Core & cavity half centre not matched.
Why 5
Root Cause (Occurance) Core & cavity half centre not matched.
 
Root Cause Analysis (Outflow)
Why 1 Defective parts are skipped from final inspection
Why 2 Part dimensionally check on sampling basis
Why 3 Operator not aware of this defect of step formation in ID.
Why 4 On job training not given to Operator
Why 5 Operator awareness of this defect is not evident
Root Cause (Outflow) Operator awareness of this defect is not evident
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceMould check sheet follow before LPA / FPA.Mr Ganesh Mhaske24/10/202424/10/2024Completed
OccuranceVerified the Guide Pins & Clamps during mould change over process.Mr Ganesh Mhaske24/10/202424/10/2024Completed
OutflowDefect matrix to display on work station.Mr Sandip Rode26/10/202425/10/2024Completed
OutflowOn the job training given to In process & Firewall operator.Mr Sandip Rode26/10/202425/10/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% Inspection at firewall through Plug Gauge.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Mould Loading Unloading WI not evident for Core Cavity Alignment .
1174_Occurance_Before.pdf
Occurance (After) Training Record to Machine as well as In process Inspection Operator for Step Formation in ID.
1174_Occurance_After.pdf
Outflow (Before) Training Record and awareness not evident to final Inspection Operator for Step formation in ID.
1174_Outflow_Before.pdf
Outflow (After) Inspection standard made for final Inspector & Operator awareness
1174_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Rebound Stop S3KJ00302O
 
12. Document Review
Documents ControlPlan, PFMEA, WISOP, InspCheckSheet
Specify Other Document NIL
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission NO ID STEP OBSERVRED.