QFR No - 8000785714
Defect Details
NC No. 8000785714
NC Date 29/04/2022
NC Submission Date
Part No. F2CK00403B
Part Name CAP NUT XF1C1_1D1
Supplier Name & Code 100106-SHARP ENGINEERS.
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-CAP NUT M22 THREAD NOGO PASS
 
1. Problem Description
Defect Description M22 X 1 X 6H THREADING NOGO PASS- CC FROM M/S SUZUKI
Detection Stage Customer End
Problem Severity Fitment
NG Quantity 1
Is Defect Repeatative? No
Defect Sketch / Photo dca2kxp4ecj4q3wvvbonetym.pptx
Supplier Communication Details
Quality Head Email ID quality@sharp-engineers.com
Plant Head/CEO Email ID kurund.ma@sharp-engineers.com
MD Email ID urkhandelwal@sharp-engineers.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
500
0
0
500
900
1900
Check Qty
500
0
0
500
0
1000
NG Qty
112
0
0
97
0
209
 
Scrap 209
Rework 0
Under Deviation 0
Containment Action
Segregation of pipeline material including ETL end material.
 
3. Process Flow
Process Flow Description
10 RM Inward Inspection 20 RM Storage 30 Parting & Drilling 40 CNC-1st Setup 50 CNC-2nd Setup 60 Plating 70 Inward Inspection 80 Final Inspection 90 PDI 100 Packing & Forwarding
 
4. Process Details
Process / Operation CNC Machining
Outsource No
Machine / Cell CNC
Machine / Cell No. 3
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachinePre-Thread Dia O/SObserved on Higher Side upto 22.10~22.20mmX
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size As per Pla
7. Root Cause Analysis (Occurance)
Why 1 M22 Threading No-go Pass observed at Customer End.
Why 2 Observed Pre-Thread Dia on Higher side upto 21.10~21.20mm
Why 3 Due to plating Allowance
Why 4
Why 5
Root Cause (Occurance) Pre-Thread Dia. On Higher Side (Due to Plating Allowance)
 
Root Cause Analysis (Outflow)
Why 1 M22 Threading No-go Pass observed at Customer End
Why 2 Not observed during final inspection stage
Why 3 No checkpoint at Final inspection
Why 4 Sample basis inspection at PDI Stage
Why 5
Root Cause (Outflow) Not Observed during Sample Basis Inspection.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccurancePre-Thread Dia taken on lower side upto 21 mm & 100% inspection added for M22x1-6H Go Gauge at Final.Mr. Dnyaneshwar30/04/2022Completed
OccuranceM22x1-6g threading gauge to be implemented on process side considering plating allowance.Mr. Mohan Jadhav03/05/2022Completed
Outflow100% Inspection at final stage.Mr. Mohan Jadhav30/04/2022Completed
OutflowPre-Thread Dia. Checking started and Dimension added in setup approval.Mr. Mohan Jadhav30/04/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 1) Pre-Thread Dia. Checking started and Dimension added in First piece approval. 2) M22x1-6g threading gauge to be implemented on process side considering plating allowance after trial. 3) 100 % inspection of NOGO from both side entry thread.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size -
10. Evidance of Countermeasure
Occurance (Before) Pre-Thread Dia. on Higher Side.
79_Occurance_Before.jpeg
Occurance (After) Pre-thread dia. taken on lower side & 100% Go gauge inspection started in final inspection.
79_Occurance_After.jpeg
Outflow (Before) No Checkpoint at final stage/Sample basis inspection
79_Outflow_Before.xlsx
Outflow (After) Checkpoint added & OPL displayed at work station
79_Outflow_After.pptx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant CNC 9/Lock Nut/E92/93
 
12. Document Review
Documents ControlPlan, InspCheckSheet
Specify Other Document OPL
 
13. Effectiveness Of Action
Reviewed Quantity 300
Reason for submission Next 3 lots found ok