QFR No - 8000787719
Defect Details
NC No. | 8000787719 |
NC Date | 17/05/2022 |
NC Submission Date | |
Part No. | F1LG00902B |
Part Name | SEAT PIPE -K86A |
Supplier Name & Code | 100929-HARSHAD ENGINEERING COMPANY |
ETL Plant | 1146-ETL Suspension Narasapura |
Defect Details | HIGHT U/SIZE.-TOTAL LENGTH LESS ISSUE |
1. Problem Description
Defect Description | K0LA seat pipe total length less issue |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 1 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo | nqppngc1jzrocztqb5vn0rur.xlsx |
Supplier Communication Details
Quality Head Email ID | qaharshad@miteshauto.com |
Plant Head/CEO Email ID | mitesh@miteshauto.com |
MD Email ID | auto.mitesh@gmail.com |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
4000
|
0
|
0
|
375
|
1100
|
5475
|
Check Qty |
4000
|
0
|
0
|
375
|
1100
|
5475
|
NG Qty |
1
|
0
|
0
|
0
|
0
|
1
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
1. 100 % sorting done at ETL 2. 100 % sorting done by length gauge checking at HEC wip & FG stock |
3. Process Flow
Process Flow Description |
---|
"10 - Raw Material Annealed and Phosphated "20-A - Cutting & 20-B- Cutting wt. "30-A MOS Application 30 -B Multistation Draw "40-A- Head Formation "40-B Inward/Incoming Inspection "50 - Rough Grinding "60-A CNC Head Turning , Facing. 60-B Facing & Boring 60-C Tapping "70A - Punching 70B-Chamfering "80-A - Finish grinding 80-B Buffing "90-A- De-burr 90-B- Final/Visual Inspection "100-A ID Cleaning Diesel 100-B - Ultrasonic cleaning "110-A- Visual Inspection at Q gate 110-B - Rust oil Application "120 - Packing & Dispatch |
4. Process Details
Process / Operation | CNC |
Outsource | No |
Machine / Cell | CNC facing & drilling machine |
Machine / Cell No. | 141, 144 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | Improper loading during facing operation | improper loading | X |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 50nos |
7. Root Cause Analysis (Occurance)
Why 1 | Total Length under size |
Why 2 | Part loaded 2.0 mm offset while facing operation |
Why 3 | while total length facing operation part not correctly loaded |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | while total length facing operation part not correctly loaded |
Root Cause Analysis (Outflow)
Why 1 | Total Length undersize |
Why 2 | total length skip from inspector |
Why 3 | 100% inspection not done for total length |
Why 4 | As per sampling inspection done |
Why 5 | |
Root Cause (Outflow) | 100% inspection not done for total length |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Training given to CNC operator for loading of parts | Kamil and Yogesh | 26/05/2022 | Completed | |
Outflow | 100% inspection started for total length | Vaibhav Sirshat | 26/05/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% inspection done for total length |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Sampling inspection for total length 124_Occurance_Before.pdf |
Occurance (After) |
100% inspection for Total Length 124_Occurance_After.pdf |
Outflow (Before) |
Not available 124_Outflow_Before.jpg |
Outflow (After) |
Training and awareness given to inspector 124_Outflow_After.jpg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | CNC |
12. Document Review
Documents | ControlPlan, WISOP |
Specify Other Document | WI and C/P |
13. Effectiveness Of Action
Reviewed Quantity | 5000 |
Reason for submission | reviewed 5000 no length issue found ok |