QFR No - 8000805167
Defect Details
NC No. 8000805167
NC Date 22/09/2022
NC Submission Date
Part No. F1BF04233M
Part Name OUTER TUBE M/C RH- K0LA DISC
Supplier Name & Code 100017-DEKSON CASTINGS LIMITED.
ETL Plant 1146-ETL Suspension Narasapura
Defect Details BLOW HOLES-CASTING BLOW HOLES
 
1. Problem Description
Defect Description blow holes
Detection Stage Inprocess
Problem Severity Aesthetic
NG Quantity 21
Is Defect Repeatative? No
Defect Sketch / Photo dr3tcca01njs00mekriaf3pk.pptx
Supplier Communication Details
Quality Head Email ID quality@dekson.co.in
Plant Head/CEO Email ID mr@dekson.co.in
MD Email ID chetandekate@dekson.co.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
200
0
0
0
300
500
Check Qty
200
0
0
0
300
500
NG Qty
2
0
0
0
0
2
 
Scrap 2
Rework 0
Under Deviation 0
Containment Action
All suspected part checked
 
3. Process Flow
Process Flow Description
Inward-Melting-Degassing-GDC-Riser Cutting-fettling grinding-GDC Q Gate- SPM-HT-VMC-BTA-Inspection- Dispatch
 
4. Process Details
Process / Operation GDC
Outsource No
Machine / Cell GDC
Machine / Cell No. 3
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodAir vent blockfound blockX
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100 %
7. Root Cause Analysis (Occurance)
Why 1 CASTING BLOW HOLES
Why 2 hot air gas not removed
Why 3 Air vent block
Why 4
Why 5
Root Cause (Occurance) Air vent block
 
Root Cause Analysis (Outflow)
Why 1 CASTING BLOW HOLES
Why 2 blow hole open after buffing
Why 3
Why 4
Why 5
Root Cause (Outflow) blow hole open after buffing
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceAir vent blockage clearDie Maint. Operator24/09/202224/09/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details check point added in inspection checksheet
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 4
10. Evidance of Countermeasure
Occurance (Before) Die air vent found block
260_Occurance_Before.jpg
Occurance (After) Die Air vent open
260_Occurance_After.jpg
Outflow (Before) No inspection checkpoint
260_Outflow_Before.jpeg
Outflow (After) inspection checkpoint added
260_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant all die
 
12. Document Review
Documents InspCheckSheet
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission blow holes open after buffing at ETL Narasapura plant so need to improve in supplier end casting process