QFR No - 8000805177
Defect Details
NC No. | 8000805177 |
NC Date | 22/09/2022 |
NC Submission Date | |
Part No. | F1BF04133M |
Part Name | OUTER TUBE M/C LH- K0LA DISC |
Supplier Name & Code | 100017-DEKSON CASTINGS LIMITED. |
ETL Plant | 1146-ETL Suspension Narasapura |
Defect Details | FITTMENT NOT OK.-BTA ID ISSUES |
1. Problem Description
Defect Description | BTA ID ISSUE |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 94 |
Is Defect Repeatative? | No |
Defect Sketch / Photo | dr3tcca01njs00mekriaf3pk.pptx |
Supplier Communication Details
Quality Head Email ID | quality@dekson.co.in |
Plant Head/CEO Email ID | mr@dekson.co.in |
MD Email ID | chetandekate@dekson.co.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
200
|
0
|
0
|
0
|
300
|
500
|
Check Qty |
200
|
0
|
0
|
0
|
300
|
500
|
NG Qty |
1
|
0
|
0
|
0
|
0
|
1
|
Scrap | 1 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
All suspected part checked |
3. Process Flow
Process Flow Description |
---|
Inward-Melting-Degassing-GDC-Riser Cutting-fettling grinding-GDC Q Gate- SPM-HT-VMC-BTA-BuffingFinal-Inspection- Dispatch |
4. Process Details
Process / Operation | BTA |
Outsource | No |
Machine / Cell | BTA |
Machine / Cell No. | 4 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Tool | BTA Tool Wear out | Tool wear out before life end | X |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | No |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 2 per hour |
7. Root Cause Analysis (Occurance)
Why 1 | FITTMENT NOT OK.-BTA ID ISSUES |
Why 2 | BTA ID having minor line mark |
Why 3 | Tool Wear out |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | Tool Wear out |
Root Cause Analysis (Outflow)
Why 1 | FITTMENT NOT OK.-BTA ID ISSUES |
Why 2 | Part skipped from inspection |
Why 3 | oversight by inspector |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | oversight by inspector |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Tool changed | Mr. Ingle | 30/09/2022 | 28/09/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | No |
Change Details | No |
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | Sampling |
Sampling | No |
Sample Size | 5 |
10. Evidance of Countermeasure
Occurance (Before) |
Tool wear out 262_Occurance_Before.jpeg |
Occurance (After) |
Tool life monitoring after tool changed 262_Occurance_After.jpeg |
Outflow (Before) |
BTA line mark 262_Outflow_Before.jpg |
Outflow (After) |
OPL Displayed 262_Outflow_After.jpeg |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | All BTA |
12. Document Review
Documents | AuditCheckSheet |
Specify Other Document | No |
13. Effectiveness Of Action
Reviewed Quantity | 1000 |
Reason for submission | reviewed 1000 number found ok |