QFR No - 8000805177
Defect Details
NC No. 8000805177
NC Date 22/09/2022
NC Submission Date
Part No. F1BF04133M
Part Name OUTER TUBE M/C LH- K0LA DISC
Supplier Name & Code 100017-DEKSON CASTINGS LIMITED.
ETL Plant 1146-ETL Suspension Narasapura
Defect Details FITTMENT NOT OK.-BTA ID ISSUES
 
1. Problem Description
Defect Description BTA ID ISSUE
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 94
Is Defect Repeatative? No
Defect Sketch / Photo dr3tcca01njs00mekriaf3pk.pptx
Supplier Communication Details
Quality Head Email ID quality@dekson.co.in
Plant Head/CEO Email ID mr@dekson.co.in
MD Email ID chetandekate@dekson.co.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
200
0
0
0
300
500
Check Qty
200
0
0
0
300
500
NG Qty
1
0
0
0
0
1
 
Scrap 1
Rework 0
Under Deviation 0
Containment Action
All suspected part checked
 
3. Process Flow
Process Flow Description
Inward-Melting-Degassing-GDC-Riser Cutting-fettling grinding-GDC Q Gate- SPM-HT-VMC-BTA-BuffingFinal-Inspection- Dispatch
 
4. Process Details
Process / Operation BTA
Outsource No
Machine / Cell BTA
Machine / Cell No. 4
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ToolBTA Tool Wear outTool wear out before life endX
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size 2 per hour
7. Root Cause Analysis (Occurance)
Why 1 FITTMENT NOT OK.-BTA ID ISSUES
Why 2 BTA ID having minor line mark
Why 3 Tool Wear out
Why 4
Why 5
Root Cause (Occurance) Tool Wear out
 
Root Cause Analysis (Outflow)
Why 1 FITTMENT NOT OK.-BTA ID ISSUES
Why 2 Part skipped from inspection
Why 3 oversight by inspector
Why 4
Why 5
Root Cause (Outflow) oversight by inspector
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceTool changedMr. Ingle30/09/202228/09/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details No
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size 5
10. Evidance of Countermeasure
Occurance (Before) Tool wear out
262_Occurance_Before.jpeg
Occurance (After) Tool life monitoring after tool changed
262_Occurance_After.jpeg
Outflow (Before) BTA line mark
262_Outflow_Before.jpg
Outflow (After) OPL Displayed
262_Outflow_After.jpeg
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All BTA
 
12. Document Review
Documents AuditCheckSheet
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission reviewed 1000 number found ok