QFR No - 8000808405
Defect Details
NC No. 8000808405
NC Date 19/10/2022
NC Submission Date
Part No. F2BF26773B
Part Name K0NA CBS OUTER TUBE CAST RH
Supplier Name & Code 101262-SUNBEAM LIGHTWEIGHTING SOLUTIO
ETL Plant 1116-ETL K-120 Suspension
Defect Details CENTRE DIST. NOT OK.-AXEL HOLE SHIFT
 
1. Problem Description
Defect Description Wall thickness variation concern reported with major rejection qty.
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 269
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID deepak.rana@sunbeamauto.com
Plant Head/CEO Email ID anoop.gupta@sunbeamauto.com
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
715
478
0
876
521
2590
Check Qty
715
478
0
870
521
2584
NG Qty
0
0
0
6
0
6
 
Scrap 6
Rework 0
Under Deviation 0
Containment Action
casting should be catch on FI stage (oil seal coller wall 100% checked by vernier)
 
3. Process Flow
Process Flow Description
"1.Alloy Preparation 2.Degassing & Defluxing 3.Casting 4.Riser Cutting 5.Fettling & Filing 6.Leak Testing 7.Final Inspection " "1.Alloy Preparation 2.Degassing & Defluxing 3.Casting 4.Riser Cutting 5.Fettling & Filing 6.Leak Testing 7.Final Inspection " 1.alloy preparation 2.degassing and defuxing 3.casting 4.riser cutting 5.fettling and filling 6.leak testing 7.final inspection
 
4. Process Details
Process / Operation casting
Outsource No
Machine / Cell gdc/domestic
Machine / Cell No. 6 and 8
5. Problem Analysis
Type Possible Cause Fact Verification Jud
Machinehydraulic pressure lowfound pressure lowX
 
6. Inspection Method Analysis (Current)
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Flash observed at parting line area
Why 2 Die was not closing
Why 3 Hydrulic pressure low
Why 4 Cylinder leakage due to core holder was shaking .
Why 5 Core holder change frequency was not deciding in pm plan cheek sheet .
Root Cause (Occurance) Core holder change frequency was not deciding in pm plan cheek sheet .
 
Root Cause Analysis (Outflow)
Why 1 Oil Seal area wall thickness ng
Why 2 Process and final inspector in this problem not captured.
Why 3 No check point avaiable in set up sheet and final work instruction sheet .
Why 4
Why 5
Root Cause (Outflow) No check point available in set up sheet and final work instruction sheet .
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceHolder change frequency decided as per PM check sheetkishore/mukesh05/11/2022Completed
Outflowcheck point add in process quality & final inspectionkishore/mukesh21/10/2022Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details 100% part inspection before dispatch
Inspection Method Instrument
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Earlier core holder frequency not defined
292_Occurance_Before.pdf
Occurance (After) Holder change frequency decided as per PM check sheet
292_Occurance_After.pdf
Outflow (Before) No check point avaiable in set up sheet and final work instruction sheet .
292_Outflow_Before.pdf
Outflow (After) check point add in process quality & final inspection
292_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant 08/kona/101262
 
12. Document Review
Documents ControlPlan, PMCheckSheet, WISOP, InspCheckSheet
Specify Other Document na
 
13. Effectiveness Of Action
Reviewed Quantity 100
Reason for submission No any re-occurance.