QFR No - 8000808405
Defect Details
NC No. | 8000808405 |
NC Date | 19/10/2022 |
NC Submission Date | |
Part No. | F2BF26773B |
Part Name | K0NA CBS OUTER TUBE CAST RH |
Supplier Name & Code | 101262-SUNBEAM LIGHTWEIGHTING SOLUTIO |
ETL Plant | 1116-ETL K-120 Suspension |
Defect Details | CENTRE DIST. NOT OK.-AXEL HOLE SHIFT |
1. Problem Description
Defect Description | Wall thickness variation concern reported with major rejection qty. |
Detection Stage | Inprocess |
Problem Severity | Fitment |
NG Quantity | 269 |
Is Defect Repeatative? | Yes |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | deepak.rana@sunbeamauto.com |
Plant Head/CEO Email ID | anoop.gupta@sunbeamauto.com |
MD Email ID |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
715
|
478
|
0
|
876
|
521
|
2590
|
Check Qty |
715
|
478
|
0
|
870
|
521
|
2584
|
NG Qty |
0
|
0
|
0
|
6
|
0
|
6
|
Scrap | 6 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
casting should be catch on FI stage (oil seal coller wall 100% checked by vernier) |
3. Process Flow
Process Flow Description |
---|
"1.Alloy Preparation 2.Degassing & Defluxing 3.Casting 4.Riser Cutting 5.Fettling & Filing 6.Leak Testing 7.Final Inspection " "1.Alloy Preparation 2.Degassing & Defluxing 3.Casting 4.Riser Cutting 5.Fettling & Filing 6.Leak Testing 7.Final Inspection " 1.alloy preparation 2.degassing and defuxing 3.casting 4.riser cutting 5.fettling and filling 6.leak testing 7.final inspection |
4. Process Details
Process / Operation | casting |
Outsource | No |
Machine / Cell | gdc/domestic |
Machine / Cell No. | 6 and 8 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Machine | hydraulic pressure low | found pressure low | X |
6. Inspection Method Analysis (Current)
Inspection Method | Sp. Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Flash observed at parting line area |
Why 2 | Die was not closing |
Why 3 | Hydrulic pressure low |
Why 4 | Cylinder leakage due to core holder was shaking . |
Why 5 | Core holder change frequency was not deciding in pm plan cheek sheet . |
Root Cause (Occurance) | Core holder change frequency was not deciding in pm plan cheek sheet . |
Root Cause Analysis (Outflow)
Why 1 | Oil Seal area wall thickness ng |
Why 2 | Process and final inspector in this problem not captured. |
Why 3 | No check point avaiable in set up sheet and final work instruction sheet . |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | No check point available in set up sheet and final work instruction sheet . |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Holder change frequency decided as per PM check sheet | kishore/mukesh | 05/11/2022 | Completed | |
Outflow | check point add in process quality & final inspection | kishore/mukesh | 21/10/2022 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | 100% part inspection before dispatch |
Inspection Method | Instrument |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
Earlier core holder frequency not defined 292_Occurance_Before.pdf |
Occurance (After) |
Holder change frequency decided as per PM check sheet 292_Occurance_After.pdf |
Outflow (Before) |
No check point avaiable in set up sheet and final work instruction sheet . 292_Outflow_Before.pdf |
Outflow (After) |
check point add in process quality & final inspection 292_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | 08/kona/101262 |
12. Document Review
Documents | ControlPlan, PMCheckSheet, WISOP, InspCheckSheet |
Specify Other Document | na |
13. Effectiveness Of Action
Reviewed Quantity | 100 |
Reason for submission | No any re-occurance. |