QFR No - 8000820733
Defect Details
NC No. 8000820733
NC Date 16/02/2023
NC Submission Date
Part No. 520HL00202
Part Name OIL LOCK COLLAR
Supplier Name & Code 101255-MAHAVIR INDUSTRIES
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-TOTAL LENGTH UNDERSIZE BY 0.20 MM
 
1. Problem Description
Defect Description Oil lock collar total length found undersize by 0.20 mm
Detection Stage Receipt
Problem Severity Fitment
NG Quantity 62
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@mahavirind.co.in
Plant Head/CEO Email ID production@mahavirind.co.in
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
1200
0
0
1840
0
3040
Check Qty
1200
0
0
1840
0
3040
NG Qty
62
0
0
1
0
63
 
Scrap 63
Rework 0
Under Deviation 0
Containment Action
All Material Segregation at Customer End
 
3. Process Flow
Process Flow Description
RM Inward- store- Parting - Bottom Chamfer-Semi finish Inward- OD Grinding Process- Plating - Final Inspection- Dispatch - Transport.
 
4. Process Details
Process / Operation Parting -ID Chamfer 2X15°
Outsource Yes
Machine / Cell Traub Section
Machine / Cell No. Traub No.03
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineMachine Part Stopper Not Proper workingPart stopper Brazing crackO
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Length under size / over size
Why 2 Resting Stopper Not Proper Working On Traub machine during parting process
Why 3 Stopper Occurs Flexible During Raw material Pipe Resting on Stopper.
Why 4 Resting Stoper Found Crack As per Attached Photograph.
Why 5
Root Cause (Occurance) Stoper crack on traub machine during parting process.2
 
Root Cause Analysis (Outflow)
Why 1 Length under size / over size
Why 2 Defective material not detect in sampling on final inspection stage During material dispatch
Why 3
Why 4
Why 5
Root Cause (Outflow) Defective material not detect in sampling on final inspection stage During material dispatch
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceOccurance- New stopper arrange on traub machine in place of old Crack stopper. Detection-New Gauge (OD AND LENGTH )Provide On Final Inspection Stage.Mr. Pralhad Bhawar / Mr.Suresh Kapgate.26/03/202326/03/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details New Combine Gauge (OD And Length )Provide On Final Inspection Stage. and Separate Snap Gauge.
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Stopper Crack Point was Not Add in Daily PM Check sheet.
370_Occurance_Before.xlsx
Occurance (After) Daily PM Check sheet Stopper Crack Point Add.
370_Occurance_After.xlsx
Outflow (Before) Sampling Purpose Snap Gauge Use
370_Outflow_Before.xlsx
Outflow (After) 100% OD and Length Purpose Combine gauge Use.
370_Outflow_After.xlsx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All Oil Lock Collar Models
 
12. Document Review
Documents ControlPlan, PMCheckSheet, PFMEA
Specify Other Document OJT
 
13. Effectiveness Of Action
Reviewed Quantity 300
Reason for submission Verified next 3 lot and found ok