QFR No - 8000822129
Defect Details
NC No. | 8000822129 |
NC Date | 28/02/2023 |
NC Submission Date | |
Part No. | 520FW04702 |
Part Name | CLUTCH HOUSING FULL FINISHED-K70 |
Supplier Name & Code | 100656-MADHURA DIE CAST PVT.LTD |
ETL Plant | 1132-ETL K-226/1 TRANSMISSION |
Defect Details | RUN OUT MORE-Ø36 MM OD R/O UPTO 0.58 MM AGAINST 0.04 |
1. Problem Description
Defect Description | Customer Complaint -Clutch DFCE Oversize up to 0.55 mm due Housing Clutch OD Ø36 mm Run out found oversize up to 0.45~0.58 mm against 0.04 mm |
Detection Stage | Customer End |
Problem Severity | Fitment |
NG Quantity | 4 |
Is Defect Repeatative? | No |
Defect Sketch / Photo |
Supplier Communication Details
Quality Head Email ID | madhuradiecast@gmail.com |
Plant Head/CEO Email ID | madhuradiecast@gmail.com |
MD Email ID | madhuradiecast@gaikegroup.in |
2. Stock Details & action taken for NG parts
Location | ETL End | Warehouse | Transit | Supplier FG | Supplier WIP | Total |
---|---|---|---|---|---|---|
Total Qty |
500
|
0
|
0
|
600
|
800
|
1900
|
Check Qty |
500
|
0
|
0
|
600
|
800
|
1900
|
NG Qty |
1
|
0
|
0
|
1
|
0
|
2
|
Scrap | 2 |
Rework | 0 |
Under Deviation | 0 |
Containment Action |
---|
100% Inspection done at ETL End by dial and mandrel with blue dot marking on OD. |
3. Process Flow
Process Flow Description |
---|
1. Casting 2.fetling 3. CNC 1st Set-up 4. CNC 2nd Set-up 5.Final Inspection. |
4. Process Details
Process / Operation | CNC 2nd Set-up |
Outsource | No |
Machine / Cell | CNC CELL |
Machine / Cell No. | CNC N0.05 |
5. Problem Analysis
Type | Possible Cause | Fact Verification | Jud |
---|---|---|---|
Man | Unskilled operator was operating machine | Level -04 operator is operate machine. | O |
Material | Burr on clamping area | Verify the component found ok | O |
Machine | Center bolt of Chuck was loose | H Sheet is verify but retightening point not updated in sheet. | X |
Tool | component was not clamp properly in jaw | Jaw pressure found not ok running condition | X |
6. Inspection Method Analysis (Current)
Inspection Method | Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
7. Root Cause Analysis (Occurance)
Why 1 | Concentricity Of Outer Diameter 36.00 mm wrt ID 22.0 mm Found 0.4 mm against 0.02 mm. |
Why 2 | n 2nd setup CNC machining Job gets loose in running. |
Why 3 | Fixture locator boss was loose. |
Why 4 | |
Why 5 | |
Root Cause (Occurance) | In machine running condition, the center bolt in the chuck was gets loose. |
Root Cause Analysis (Outflow)
Why 1 | Inspector checking method was sampling basis |
Why 2 | gauging checking frequency was less |
Why 3 | |
Why 4 | |
Why 5 | |
Root Cause (Outflow) | gauging checking frequency was less |
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type | Countermeasure Details | Responsibility | Target Date | Actual Date | Status |
---|---|---|---|---|---|
Occurance | Additional tightening arrangement by Grub Screw provided for Centre bolt of locator boss to avoid the centre bolt loose issue | PRODUCTION supervisor | 10/03/2023 | 08/03/2023 | Completed |
Outflow | Training and awareness given to inspector for checking 100% Concentricity Of Outer Diameter 36.00. wrt ID 22.0 With reading on job in micron. | QA Engineer | 10/03/2023 | 08/03/2023 | Completed |
9. Inspection Method After Customer Complaint
Change In Inspection System | Yes |
Change Details | Started 100% Concentricity Of Outer Diameter 36.00. wrt ID 22.0 With reading on job in micron |
Inspection Method | Sp. Gauge |
Other Inspection Method | |
Check Point at Final Inspection | Yes |
Checking Freq. | 100% |
Sampling | No |
Sample Size | 100% |
10. Evidance of Countermeasure
Occurance (Before) |
JH Sheet is not updated for Centre bolt retightening 381_Occurance_Before.pdf |
Occurance (After) |
JH Sheet is updated for Centre bolt retightening frequency and method 381_Occurance_After.pdf |
Outflow (Before) |
Runout checking frequency is sample basis. 381_Outflow_Before.pdf |
Outflow (After) |
Runout checking frequency change sample to 100% and reading mentioned on part. 381_Outflow_After.pdf |
11. Horizontal Deployment
Horizontal Deployment Required | Yes |
Applicable Machine / Model / Plant | Machine N0.01 |
12. Document Review
Documents | ControlPlan, JHCheckSheet, InspCheckSheet |
Specify Other Document | OPL |
13. Effectiveness Of Action
Reviewed Quantity | 2000 |
Reason for submission | OK |