QFR No - 8000822129
Defect Details
NC No. 8000822129
NC Date 28/02/2023
NC Submission Date
Part No. 520FW04702
Part Name CLUTCH HOUSING FULL FINISHED-K70
Supplier Name & Code 100656-MADHURA DIE CAST PVT.LTD
ETL Plant 1132-ETL K-226/1 TRANSMISSION
Defect Details RUN OUT MORE-Ø36 MM OD R/O UPTO 0.58 MM AGAINST 0.04
 
1. Problem Description
Defect Description Customer Complaint -Clutch DFCE Oversize up to 0.55 mm due Housing Clutch OD Ø36 mm Run out found oversize up to 0.45~0.58 mm against 0.04 mm
Detection Stage Customer End
Problem Severity Fitment
NG Quantity 4
Is Defect Repeatative? No
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID madhuradiecast@gmail.com
Plant Head/CEO Email ID madhuradiecast@gmail.com
MD Email ID madhuradiecast@gaikegroup.in
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
500
0
0
600
800
1900
Check Qty
500
0
0
600
800
1900
NG Qty
1
0
0
1
0
2
 
Scrap 2
Rework 0
Under Deviation 0
Containment Action
100% Inspection done at ETL End by dial and mandrel with blue dot marking on OD.
 
3. Process Flow
Process Flow Description
1. Casting 2.fetling 3. CNC 1st Set-up 4. CNC 2nd Set-up 5.Final Inspection.
 
4. Process Details
Process / Operation CNC 2nd Set-up
Outsource No
Machine / Cell CNC CELL
Machine / Cell No. CNC N0.05
5. Problem Analysis
Type Possible Cause Fact Verification Jud
ManUnskilled operator was operating machineLevel -04 operator is operate machine.O
MaterialBurr on clamping areaVerify the component found okO
MachineCenter bolt of Chuck was looseH Sheet is verify but retightening point not updated in sheet.X
Toolcomponent was not clamp properly in jawJaw pressure found not ok running conditionX
 
6. Inspection Method Analysis (Current)
Inspection Method Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
7. Root Cause Analysis (Occurance)
Why 1 Concentricity Of Outer Diameter 36.00 mm wrt ID 22.0 mm Found 0.4 mm against 0.02 mm.
Why 2 n 2nd setup CNC machining Job gets loose in running.
Why 3 Fixture locator boss was loose.
Why 4
Why 5
Root Cause (Occurance) In machine running condition, the center bolt in the chuck was gets loose.
 
Root Cause Analysis (Outflow)
Why 1 Inspector checking method was sampling basis
Why 2 gauging checking frequency was less
Why 3
Why 4
Why 5
Root Cause (Outflow) gauging checking frequency was less
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceAdditional tightening arrangement by Grub Screw provided for Centre bolt of locator boss to avoid the centre bolt loose issuePRODUCTION supervisor10/03/202308/03/2023Completed
OutflowTraining and awareness given to inspector for checking 100% Concentricity Of Outer Diameter 36.00. wrt ID 22.0 With reading on job in micron.QA Engineer10/03/202308/03/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Started 100% Concentricity Of Outer Diameter 36.00. wrt ID 22.0 With reading on job in micron
Inspection Method Sp. Gauge
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) JH Sheet is not updated for Centre bolt retightening
381_Occurance_Before.pdf
Occurance (After) JH Sheet is updated for Centre bolt retightening frequency and method
381_Occurance_After.pdf
Outflow (Before) Runout checking frequency is sample basis.
381_Outflow_Before.pdf
Outflow (After) Runout checking frequency change sample to 100% and reading mentioned on part.
381_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Machine N0.01
 
12. Document Review
Documents ControlPlan, JHCheckSheet, InspCheckSheet
Specify Other Document OPL
 
13. Effectiveness Of Action
Reviewed Quantity 2000
Reason for submission OK