QFR No - 8000823929
Defect Details
NC No. 8000823929
NC Date 20/03/2023
NC Submission Date
Part No. F2FA01200B
Part Name FORK PIPE RAW K23A (W/O HARDENING)
Supplier Name & Code 101066-TUBE INVESTMENTS OF INDIA LIMI
ETL Plant 1116-ETL K-120 Suspension
Defect Details NOT AS PER SPECIFICATION-HARDNESS & THICKNESS NG
 
1. Problem Description
Defect Description 1) Fork pipe Hardness (28±4HRC) observed up to 12 ~15 HRC. 2) Thickness variation observed up to 0.35mm.
Detection Stage Inprocess
Problem Severity Safety
NG Quantity 5
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID AmitVD@tii.murugappa.com
Plant Head/CEO Email ID guptaajay@tii.murugappa.com
MD Email ID mukeshahuja@tii.murugappa.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
52407
0
0
0
0
52407
Check Qty
52407
0
0
0
0
52407
NG Qty
5945
0
0
0
0
5945
 
Scrap 5945
Rework 0
Under Deviation 0
Containment Action
100 % Inspection done by using Eddy Sorter machine in available Qty. 52407 Nos. at ETL End.
 
3. Process Flow
Process Flow Description
Drawing- Tempering-Straightning-Edyy Current Testing-Cutting-Final Inspection.
 
4. Process Details
Process / Operation Tempering Process
Outsource No
Machine / Cell Online Tempering Machine
Machine / Cell No. 13A106
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachinePower - 203kw , Speed 16 MPM Speed reduced by 4 MPM1. Hardness found 22-25HRC and not matching with failed part Hardness 2. No visual differenceO
MachinePower -200kw , Speed 14 MPM Speed reduced by 6 MPM1. Hardness found 22-25HRC and not matching with failed part Hardness 2. No visual differenceO
MachineTube Jerk: Tube holding 2 -3 sec and repeat the same for 3 times in same tubeHardness found okO
MachinePower -241KW , Speed -20MPM Power increased by 40KW1. Hardness found 23-28HRC and not matching with failed part Hardness 2. No visual differenceO
MachineSpeed -20mpm , Power -203KWHardness found okO
MachineTube Stuck-up: Tube holding time 5- 6 sec1. Hardness found 14-15 HRC and matching with failed part Hardness 2. end portion is hardness foundX
MachinePower - 230 KW ,Speed -20MPM Power increased by 30KW1. Hardness found 24-28HRC and not matching with failed part Hardness 2. No visual differenceO
 
6. Inspection Method Analysis (Current)
Inspection Method Pokayoke
Other Inspection Method
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size /JOB ORDER
7. Root Cause Analysis (Occurance)
Why 1 Tube bend during process
Why 2 Tube low hardness
Why 3 Tube low hardness at temering
Why 4 Tube excess tempering
Why 5 Tube struck up at tempering for more than 5 seconds
Root Cause (Occurance) Tube struck up at tempering for more than 5 seconds
 
Root Cause Analysis (Outflow)
Why 1 Tube bend during the process
Why 2 Tube low hardness
Why 3 NG tube mixed with ok tube
Why 4 No identification of NG tube
Why 5
Root Cause (Outflow) No identification of NG tube
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowSeparate bucket provided for NG tubesMr. Rajkumar30/03/202330/03/2023Completed
Occurance1. Interlocking of tube struck up (more than 3 seconds) and tempering coil power offMr. Rajkumar30/03/202330/03/2023Completed
OutflowAuto Paint spray system introduced during tube struck up in tempering line more than 3 secondsMr. Rajkumar30/03/202329/03/2023Completed
Outflow.Hardness verification point added at tempering stage for each job orderMr. Rajkumar30/03/202329/03/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System Yes
Change Details Hardness verification added during tempering
Inspection Method Other
Other Inspection Method Hardness verificatio
Check Point at Final Inspection Yes
Checking Freq. Sampling
Sampling No
Sample Size /job order
10. Evidance of Countermeasure
Occurance (Before) NIL
393_Occurance_Before.pdf
Occurance (After) 1. Interlocking of tube struck up (more than 3 seconds) and tempering coil power off 2. Auto Paint spray system introduced during tube struck up in tempering line more than 3 seconds
393_Occurance_After.pdf
Outflow (Before) NIL
393_Outflow_Before.pdf
Outflow (After) 1. Hardness verification point added at the tempering stage for each job order 2. Separate buckets provided for NG tubes
393_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant Online Tempering machines at PAN TPI
 
12. Document Review
Documents WISOP, InspCheckSheet
Specify Other Document No
 
13. Effectiveness Of Action
Reviewed Quantity
Reason for submission