QFR No - 8000833477
Defect Details
NC No. 8000833477
NC Date 20/06/2023
NC Submission Date
Part No. S1GD01726B
Part Name INNER TUBE CHAMFERED K0LA
Supplier Name & Code 101273-SAPTAGIRI ENGINEERING PRIVATE
ETL Plant 1136-ETL Suspension Sanand
Defect Details LESS CHAMFER-CHAMFER NG
 
1. Problem Description
Defect Description ID gauge not qualifying (Chamfer NG and bend).
Detection Stage Inprocess
Problem Severity Fitment
NG Quantity 90
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID quality@saptagirigroup.in
Plant Head/CEO Email ID production@saptagirigroup.in
MD Email ID
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
3000
3000
0
0
2000
8000
Check Qty
3000
3000
0
0
2000
8000
NG Qty
90
0
0
0
0
90
 
Scrap 0
Rework 90
Under Deviation 0
Containment Action
100 % material verified by visual
 
3. Process Flow
Process Flow Description
Raw Tube + Cutting + Both Side chamfer + Inspection
 
4. Process Details
Process / Operation Chamfer
Outsource No
Machine / Cell 01
Machine / Cell No. 01
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MachineClamp loosedNo Rigid clamping providedX
ManInspector not awareInspector not aware about the chamferX
ToolInsert Ware out or brokenNo Insert warn out and brokenO
MachineUneven tube cutting doneNo uneven cutting done its parallelism observed within 0.1 mmO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100 %
7. Root Cause Analysis (Occurance)
Why 1 Less Chamfer / Chamfer Uneven
Why 2 W.r.t. center outer tube clamping alignment disturb
Why 3 O/t Clamping plate loosed
Why 4 Capsule slot given for bolt locking of the clamping plate
Why 5
Root Cause (Occurance) Capsule slot given for bolt locking of the clamping plate
 
Root Cause Analysis (Outflow)
Why 1 Less Chamfer / Chamfer Uneven
Why 2 Inspector Not aware about defect
Why 3
Why 4
Why 5
Root Cause (Outflow) Inspector Not aware about defect
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OutflowAwareness training given to inspectorMr. Dhiraj Patil27/06/202326/06/2023Completed
OccuranceRigid bolt engage with clamping plate including spring tension washer to avoided clamping plate loosed issueMr. Pravin Jonwal27/06/202326/06/2023Completed
OccuranceFor verification of O/t clamping plate point has added in daily machine check sheetMr. Pravin Jonwal27/06/202326/06/2023Completed
Outflow100 % visul inspection started as per one point lesson and Q alert Display at work placeMr. Dhiraj Patil27/06/202326/06/2023Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details Na
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection Yes
Checking Freq. 100%
Sampling No
Sample Size 100%
10. Evidance of Countermeasure
Occurance (Before) Implementation & Action for Less chamfer
491_Occurance_Before.pptx
Occurance (After) Implementation & Action for Less chamfer
491_Occurance_After.pptx
Outflow (Before) Implementation & Action for Less chamfer
491_Outflow_Before.pptx
Outflow (After) Implementation & Action for Less chamfer
491_Outflow_After.pptx
 
11. Horizontal Deployment
Horizontal Deployment Required Yes
Applicable Machine / Model / Plant All type of Inner Tube
 
12. Document Review
Documents PokayokeCheckSheet
Specify Other Document Na
 
13. Effectiveness Of Action
Reviewed Quantity 3
Reason for submission chamfer NG