QFR No - 8000857899
Defect Details
NC No. 8000857899
NC Date 08/01/2024
NC Submission Date
Part No. 520HL00202
Part Name OIL LOCK COLLAR
Supplier Name & Code 100176-GKN SINTER METALS PRIVATE LIMI
ETL Plant 1117-ETL K-228/9 Suspension
Defect Details NOT AS PER SPECIFICATION-HEAVY RUSTY
 
1. Problem Description
Defect Description Heavy rusty
Detection Stage Receipt
Problem Severity Aesthetic
NG Quantity 1300
Is Defect Repeatative? Yes
Defect Sketch / Photo
Supplier Communication Details
Quality Head Email ID Rajendra.Sethiya@gknpm.com
Plant Head/CEO Email ID Pratik.Dharangaonkar@gknpm.com
MD Email ID Rajesh.Mirani@gknpm.com
2. Stock Details & action taken for NG parts
Location ETL End Warehouse Transit Supplier FG Supplier WIP Total
Total Qty
7500
12000
0
0
0
19500
Check Qty
7500
12000
0
0
0
19500
NG Qty
400
0
0
0
0
400
 
Scrap 400
Rework 0
Under Deviation 0
Containment Action
All stock lying at ETL segregated , Quality alert raised at Concerned Area
 
3. Process Flow
Process Flow Description
Forming - Sintering - Barreling - Steam Treatment - PDI
 
4. Process Details
Process / Operation Steam Treatment
Outsource No
Machine / Cell NA
Machine / Cell No. NA
5. Problem Analysis
Type Possible Cause Fact Verification Jud
MethodInspection Standard not availableInspection standard verified, available at concerned areaO
ManUntrained OperatorOperator skill matrix is okO
MaterialParts Metallurgy NGParts are OK to the metallurgical check and found okO
 
6. Inspection Method Analysis (Current)
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size 5
7. Root Cause Analysis (Occurance)
Why 1 Rust observed on part`s surface
Why 2 Part got rust as it came in contact with Moisture
Why 3 Insufficeint protection for parts getting Rust due to Monsoon season
Why 4 Parts been handled in MS Basket not covered with VCI Bags
Why 5
Root Cause (Occurance) As during Mansoon season part came in contact with Moisture due to which part got Rusted during Storage.
 
Root Cause Analysis (Outflow)
Why 1 Rust observed on part`s surface
Why 2 Didn’t get detected during Final Inspection
Why 3 Part got rust after Dispatch/Storage
Why 4
Why 5
Root Cause (Outflow) During In-process & Final Inspection parts found OK & got rusted during Storage at warehoue.
 
8. Countermeasure ( Occurrence , Outflow & System side Actions )
Type Countermeasure Details Responsibility Target Date Actual Date Status
OccuranceDuring Mansoon season parts to be handled in VCI Bags in MS Baskets to ensure parts doesn’t came in contact with moisture.Vijay Thorat17/02/2024Completed
OutflowAfter action implementation 100nos samples to be kept for Observation, which need to check once a week for 4months.Rohan G29/02/2024Completed
 
9. Inspection Method After Customer Complaint
Change In Inspection System No
Change Details After action implementation 100nos samples to be kept for Observation, which need to check once a week for 4months.
Inspection Method Other
Other Inspection Method Visual
Check Point at Final Inspection No
Checking Freq. Sampling
Sampling No
Sample Size 5
10. Evidance of Countermeasure
Occurance (Before) No polybags for MS basket
628_Occurance_Before.pdf
Occurance (After) During Monsoon season parts to be handled in VCI Bags in MS Baskets to ensure parts doesn’t came in contact with moisture.
628_Occurance_After.pdf
Outflow (Before) NA
628_Outflow_Before.pdf
Outflow (After) NA
628_Outflow_After.pdf
 
11. Horizontal Deployment
Horizontal Deployment Required No
Applicable Machine / Model / Plant NA
 
12. Document Review
Documents PFMEA, WISOP, AuditCheckSheet
Specify Other Document NA
 
13. Effectiveness Of Action
Reviewed Quantity 1000
Reason for submission Found ok